There are 3 owner-reported speed control & cruise complaints for the 2013 Buick Enclavein NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
WHILE DRIVING MY 2013 BUICK ENCLAVE TRACTION CONTROL, SERVICE STABILI TRACK FLASHES ACROSS DASBOARD. THE CHECK ENGINE LIGHT COMES ON AND ENGINE SPEED IS DRASTICALLY REDUCED. CAR DOES NOT ACCELERATE PROPERLY AND RPMS ARE NOT PRODUCING SPEED. CAR IS LETHARGIC AND SIGNS BEGIN WITHOUT WARNING. ONCE ENGINE IS TURNED OFF AND TURNED BACK ON TRACTION CONTROL RESTS AND DISPLAY MESSAGES DISAPPEAR BUT CHECK ENGINE LIGHT REMAINS ON. TEMPERATURE OR WEATHER OR TYPE OF ROAD YOU ARE DRIVING ON DOES NOT PLAY A FACTOR IN DEFECT OF TRACTION CONTROL STABILI TRACK.
ON 3/21/18 I WAS PULLING OUT OF A GAS STATION TO HEAD TO WORK. MY TRACTION CONTROL LIGHT LIT UP AS WELL AS MY ENGINE LIGHT. WARNINGS WENT ACROSS MY DASH STATING "TRACTION CONTROL OFF" "SERVICE STABILITRACK" "ENGINE POWER REDUCED" I COULDN'T GO OVER 40MPH. I MADE IT BACK TO WORK. AFTER WORK ONLY THE ENGINE LIGHT WAS ON. THE NEXT DAY I DROVE IT AND BY THE AFTERNOON THE ENGINE LIGHT HAD GONE OFF. THIS MORNING, 3/23/18 I DROVE TO WORK WITHOUT ANY COMPLICATIONS. DUE TO WEATHER WE CLOSED OUR OFFICE EARLY. I PULLED OUT OF THE PARKING LOT AND MY TRACTION CONTROL LIT UP AS WELL AS MY ENGINE LIGHT. ALL THREE WARNINGS WENT ACROSS MY DASH AGAIN AND THIS TIME I COULD NOT GO ABOVE 20MPH. I MADE IT HOME WITH MY FLASHERS ON. ONCE I GOT HOME I LET MY CAR SIT FOR A COUPLE HOURS AND THEN TOOK IT AROUND THE BLOCK. AGAIN ONLY MY ENGINE LIGHT WAS ON. WE WILL TAKE IT TO THE SHOP ONCE THE WEATHER CLEARS.
TL* THE CONTACT OWNS A 2013 BUICK ENCLAVE. WHILE DRIVING VARIOUS SPEEDS, THE VEHICLE SUDDENLY JERKED AND THE SPEED REDUCED TO 20 MPH. THE CHECK ENGINE AND STABILITY TRAC MALFUNCTION WARNING INDICATORS ILLUMINATED. THE CONTACT PULLED OVER TO THE SIDE OF THE ROAD. THE CONTACT TURNED OFF AND RESTARTED THE ENGINE, AND THE VEHICLE RETURNED TO NORMAL. THE VEHICLE WAS TAKEN TO THE DEALER (ALEXANDER BUICK GMC CADILLAC, 1501 VENTURA BLVD, OXNARD, CA 93036) FOUR TIMES WHERE IT WAS DIAGNOSED THAT THE KEY FOB ALARM NEEDED TO BE REMOVED. THE VEHICLE WAS REPAIRED. THE FAILURE RECURRED SEVERAL OTHER TIMES. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS CONTACTED. THE APPROXIMATE FAILURE MILEAGE WAS 70,000. THE VIN WAS NOT AVAILABLE.
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 25, 2026