There are 7 owner-reported engine complaints for the 2011 Ford Expeditionin NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
The engine is blown at 125k miles when all servicing and maintenance was done at the dealership. Somewhere around 50k to 60k miles, I complained to the dealership about a ticking noise from the engine and was told multiple times it was "normal with this engine". Well this engine blew while I was on my way to take the kids to school. I was on the interstate/bypass and was by some miracle able to get the 7-11. I was driving and all of a sudden, it sounded like there was squirrel under the hood. I had to have it towed to the dealership because it was not driveable and they told me the engine was no longer good and was blown. They said it would cost me $10k and I would be better off buying a new vehicle. There was no engine light or anything that came on until it blew. The only "warning" I had was the slight ticking noise that came from the engine, but when mentioned to the dealership, I was told that it was normal with this engine.
CAMSHAFT ROLLER BEARINGS SEIZED AND SCORED THE CAMSHAFT, REQUIRING A TOP END REPLACEMENT. THE VEHICLE HAD LESS THAN 95000 MILES. THIS THE SECOND EXPEDITION REQUIRING THIS ENGINE WORK. MY FIRST EXPEDITION REQUIRED A COMPLETE ENGINE REPLACEMENT DUE TO THE SAME ISSUE
UPON ENGAGING THE CRUISE CONTROL WHILE IN MOTION AT 65MPH (HIGHWAY) AND GOING UP A BRIDGE THE VEHICLE ACCELERATED WITH ACCELERATOR BEING STUCK ON THE FLOOR (BOTTOMED OUT) BRAKING BECAME INEFFECTIVE AT THAT SPEED. AFTER A MAJOR EFFORT WAS ABLE TO PULL OVER. PUTTING IN NEUTRAL MADE THE VEHICLE IDLE AT VERY HIGH RPM, DID NOT DISENGAGE THE ACCELERATOR. ONLY AFTER SHUTTING THE ENGINE OFF IN N AND PUTTING THE VEHICLE IN P FOLLOWED BY RESTARTING SOLVED THE ISSUE. SECOND TIME THIS OCCURRED WAS AT 55MPH (LOCAL HIGHWAY) FLAT ROAD, SAME OBSERVATIONS. BRIEFLY DISCONNECTING AND RECONNECTING CONTACT DID NOT SOLVE THE PROBLEM. VERY HIGH IDLE IN N AND ONLY AFTER PUTTING THE VEHICLE IN P AFTER SHUTTING DOWN, THE PHENOMENON WAS RESOLVED. ONLY OBSERVED WHILE USING CRUISE CONTROL. IN BOTH CONDITIONS ROAD WAS DRY WITH NO PRECIPITATION
TL* THE CONTACT OWNS A 2011 FORD EXPEDITION. WHILE DRIVING AT VARIOUS SPEEDS, THE ENGINE SHOOK UNCONTROLLABLY WITHOUT WARNING. THE FAILURE OCCURRED WHENEVER THE BRAKE PEDAL WAS DEPRESSED. THE DEALER STATED THAT THE VEHICLE WAS BUILT WITH A FAULTY ENGINE. THE MANUFACTURER WAS NOTIFIED, BUT OFFERED NO REMEDY. THE VIN WAS UNAVAILABLE. THE FAILURE MILEAGE WAS 131,476. UPDATED 02/05/16*LJ
TL* THE CONTACT OWNS A 2011 FORD EXPEDITION. THE CONTACT STATED THAT WHILE COMING TO A STOP, THE VEHICLE JERKED AND MADE AN ABNORMAL NOISE COMING FROM THE ENGINE. THE FAILURE RECURRED SEVERAL TIMES. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THE FAILURE WAS NOT DETERMINED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 110,000.
TL* THE CONTACT OWNS A 2011 FORD EXPEDITION. THE CONTACT SMELLED A STRONG FUEL ODOR INSIDE THE VEHICLE. THE CONTACT ALSO STATED THAT THE FAN MADE AN INTERMITTENT CLICKING NOISE ON MULTIPLE OCCASIONS WHEN THE VEHICLE WAS BEING DRIVEN. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE APPROXIMATE FAILURE MILEAGE WAS 60,000.
TL* THE CONTACT OWNS A 2011 FORD EXPEDITION. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 40 MPH THE REAR WHEELS LOCKED MOMENTARILY. THE FAILURE CONTINUED TO RECUR ON AN INTERMITTENT BASIS. THE VEHICLE ALSO STALLED DURING ONE OF THE FAILURES. THE CONTACT ALSO STATED THAT THE VEHICLE WAS A RENTAL AND WAS TOWED BACK TO THE RENTAL AGENCY AFTER STALLING. THE CONTACT WAS NOT AWARE IF THE VEHICLE WAS EVER TAKEN TO HAVE THE FAILURE DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS 7,000. THE VIN WAS UNAVAILABLE.
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 26, 2026