There are 10 owner-reported fuel system complaints for the 2006 Ford F-250in NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
I OWN A 2006 FORD F 250, ON SATURDAY WHILE DRIVING THE VEHICLE ON THE HIGHWAY I NOTICED A WET STREAK BEHIND ME SO I PULLED OVER AND NOTICED GAS GUSHING OUT OF A HOLE IN THE TANK. FORTUNATELY I WAS IN A RURAL AREA CLOSE TO HOME, SO I DROVE IT THE REST OF THE WAY HOME AND PARKED IT IN A FIELD, AWAY FROM ANY BUILDINGS TO ALLOW THE 30+ GALLONS OF GAS TO DRAIN OUT. THE CAUSE OF THE LEAK WAS ONE OF THE STRAPS THAT SECURES THE FUEL TANK BROKE (RUSTED IN HALF) AND THE GAS TANK DROPPED DOWN AND WAS DRAGGING AGAINST THE HIGHWAY. I ATTACHED A PHOTO OF THE STRAP THAT BROKE
WAS TRAVELING DOWN INTERSTATE 24 AFTER JUST FUELING UP WHEN HIT A ROUGH SPOT ON THE HIGHWAY AND THE FUEL TANK DROPPED OUT OF THE TRUCK LEAVING ME AND MY STEPSON STRANDED ON THE SIDE OF THE INTERSTATE COST ME 1200 DOLLARS TO BE TOWED HOME NOT TO MENTION WHAT THE REPAIR COST ARE GOING TO COST ME
TL* THE CONTACT OWNS A 2006 FORD F-250. THE CONTACT STATED WHILE DRIVING AT 35 MPH, THERE WAS AN ABNORMAL SOUND COMING FROM THE VEHICLE. THE CONTACT MERGED TO THE SHOULDER OF THE ROAD AND NOTICED THAT THE FUEL TANK STRAP FAILED CAUSING THE FUEL TANK TO HANG. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 180,000.
TRUCK STALLED AT INTERSECTION. COMPLETE POWER OUTAGE, NO BRAKES, ETC. MANAGES TO RESTART. PROBLEM RECURRED TWO ADDITIONAL TIMES. I LIMPED TO A LOCAL MECHANIC SHOP WHO SCANNED THE ENGINE CODES. HE TOLD ME IT WAS THE THROTTLE BODY AND CHARGED ME $550.00 TO REPLACE IT. TRUCK HAD 47,000 ON IT AT THE TIME. IN MY OPINION THIS PART SHOULD LAST WELL INTO THE 100,000 MILE MARK. *TR
TL* THE CONTACT OWNS A 2006 FORD F-250. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 65 MPH, THE VEHICLE STALLED. THE VEHICLE WAS TOWED TO THE DEALER WHERE THE CONTACT WAS ADVISED THAT THE FUEL PUMP, CIRCUIT AND THE FUEL INJECTORS WOULD HAVE TO BE REPLACED. THE VEHICLE WAS REPAIRED BUT TO NO AVAIL. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 106,000. *TR
THE FICM (FUEL INJECTOR CONTROL MODULE) ON THE 6.0L POWERSTROKES ARE A KNOWN ITEM TO FAIL. THEY LOSE VOLTAGE AND MAKE INJECTORS NOT WORK, WHICH SHUTS OFF THE VEHICLE. THIS CAN HAPPEN AT ANY TIME WHILE AT AN IDLE OR GOING DOWN THE HIGHWAY. ONCE THIS HAPPENS, THE TRUCK SHUTS OFF AND YOU LOSE POWER STEERING AND BRAKING ABILITY. MINE SHUT OFF WHILE GOING DOWN THE ROAD SEVERAL TIMES NOW, BUT FORD DOES NOT WANT TO WARRANTY IT. MY SMALL TOWN FORD DEALERSHIP REPLACES SEVERAL OF THESE PARTS A WEEK. DOES SOMEONE HAVE TO DIE FOR THEM TO ISSUE A RECALL ON THESE? *TR
2/15/10 ~ FUEL REGULATOR CHANGED. 2/16/10 ~ SENSOR AND CONNECTOR CHANGED. 3/1/2010~ FUEL INJECTORS REPLACED, EGR COLLOR CONNECTOR, HIGH PRESSURE OIL PUMP PRELACED. NOW 1 YEAR LATER ALL INJECTORS NEED TO BE REPLACED AGAIN.
TL* THE CONTACT OWNS A 2006 FORD F250. THE CONTACT ATTEMPTED TO ACCELERATE FROM A COMPLETE STOP, BUT THERE WAS NO ENGINE POWER. THE VEHICLE WAS TOWED TO THE DEALER WHERE THE FUEL FILTER WAS REPLACED. THE FAILURE REOCCURRED TWO DAYS AFTER THE REPAIR. THE CONTACT WAS ABLE TO DRIVE THE VEHICLE BACK TO THE DEALER FOR DIAGNOSIS. THE TECHNICIAN INFORMED THE CONTACT THAT THE FAILURE COULD POSSIBLY BE CONTRIBUTED TO THE FUEL INJECTORS. THE VEHICLE WAS IN THE PROCESS OF BEING REPAIRED. THE VEHICLE HAD NOT BEEN DRIVEN FOR ONE YEAR DUE TO THE INTERMITTENT FAILURES AND INSUFFICIENT REPAIRS. THE FAILURE OCCURRED FOUR DIFFERENT TIMES. THE FAILURE MILEAGE WAS APPROXIMATELY 120,000. THE VIN WAS UNAVAILABLE. UPDATED 12/10/10. *LJ
TL* THE CONTACT OWNS A 2006 FORD F-250 SD. THE CONTACT STATED THAT WHILE REFUELING, FUEL SPEWED FROM THE FILLER NECK. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THE TECHNICIAN DIAGNOSED THAT THE CHECK VALVE WAS STICKING AND AS RESULT, THE FUEL PUMP NEEDED TO BE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 56,935 AND THE CURRENT MILEAGE WAS 58,827.
DT*: THE CONTACT STATED WITHOUT WARNING, WHILE DRIVING AT ANY SPEED, THE ENGINE WOULD CUT OUT AND STALL WHILE THE ACCELERATOR PEDAL WAS BEING RELEASED. THE VEHICLE RESTARTED AFTER 15 MINUTES. THE DEALERSHIP DETERMINED THE INJECTORS WENT OUT, CAUSING DIESEL TO GET INTO THE OIL. THE INJECTORS WERE REPLACED AND THE OIL CHANGED. SINCE THE REPAIRS, THE TRANSMISSION SLIPS WHILE PULLING A HORSE TRAILER OVER A MOUNTAIN. THE VEHICLE HAS NOT BEEN RETURNED TO THE DEALERSHIP.
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 26, 2026