There are 50 owner-reported engine complaints for the 1998 Ford Taurusin NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
AFTER DRIVING ABOUT A MILE, THE AIR CONDITIONING STOPPED AND BLACK SMOKE CAME OUT OF THE HOOD. STOPPED THE CAR AND THOUGHT OF OPENING THE HOOD BUT SAW FLAMES. THREE ADULTS AND TWO CHILDREN (5 AND 2 YRS OLD) GOT OUT OF THE CAR. CALLED POLICE AND FIRE SERVICE. BY THE TIME THEY ARRIVE, THE CAR WAS IN FLAMES. THE ENGINE AND FRONT ROW SEATS WERE TOTALLY BURNT. THE CAR WAS A TOTAL LOSS. THERE WAS NO WAY TO DETERMINE THE REASON FOR THE (MYSTERIOUS) FIRE. THIS HAPPENED IN MIAMI, FLORIDA. *TR
TL*THE CONTACT OWNS A 1998 FORD TAURUS. THE CONTACT STATED THAT AFTER PARKING THE VEHICLE AND TURNING IT OFF, IT WOULD NOT START AGAIN. THE FAILURE OCCURRED INTERMITTENTLY. NO WARNING LIGHTS ILLUMINATED ON THE INSTRUMENTAL PANEL. THE VEHICLE WAS INSPECTED BY A DEALER AND THEY INFORMED HER THAT THEY WERE UNABLE TO DIAGNOSE THE FAILURE. THE VEHICLE HAD NOT BEEN REPAIRED. THE FAILURE MILEAGE WAS APPROXIMATELY 142,000.
TL* THE CONTACT OWNS A 1998 FORD TAURUS. THE VEHICLE WOULD OCCASIONALLY EXHIBIT A NO-START CONDITION. SHE ALSO NOTICED THE CHECK ENGINE WARNING LIGHT ILLUMINATED ON THE INSTRUMENT CONTROL PANEL. THE VEHICLE HAS NOT BEEN DIAGNOSED BY THE DEALERSHIP. THE CURRENT AND FAILURE MILEAGES WERE 167000. UPDATED 12/7/09 *CN THE CONSUMER STATED THE ENGINE WOULD BECOME EXCESSIVELY HOT. UPDATED 12/08/09*JB
FORD TAURUS 1998 ENGINE COOLANT RESERVOIR (PLASTIC CONTAINER) SPRUNG A LEAK ON THE BOTTOM SIDE. NO INDICATION OF ANY RUBBING AGAINST ANYTHING. I ORDERED A REPLACEMENT FROM AN ON-LINE INTERNET PARTS WHOLESALER AND THEY SAID THEY HAD MANY ORDERS FOR REPLACEMENT FORD TAURUS ENGINE COOLANT RESERVOIR BOTTLES. I NEVER HAD SUCH A PROBLEM ON ANY PREVIOUS CAR THAT I HAVE OWED BEFORE. *TR
ENGINE OIL IS LEAKING ON EXHAUST SYSTEM FROM BACK SIDE OF ENGINE. STRONG SMELL AND OIL ON GROUND' 81,000 MILES ON VEHICLE. I PURCHASED VEHICLE NEW. REPLACED VALVE COVER GASKETS. STILL LEAKING OIL. *TR
NO HEAT. TOOK OUR 1998 FORD TAURUS 6CYL.,3.0L,182FI VEHICLE TO DEALER WITH COMPLAINT OF NO HEAT. I AM TOLD FROM THE FORD SERVICE ADVISOR THAT THERE IS RUST IN THE COOLANT SYSTEM CAUSED BY A METAL ALLERGY REACTION FROM THE WATER PUMP IMPELLER BLADE AND THE ANTIFREEZE COOLANT IN THE SYSTEM WHICH CAUSE RUST THE INSIDE OF THE ENGINE, FREEZE PLUGS, HEATER CORE, THERMOSTAT AND EVENTUALLY CAUSE THE ENGINE TO OVERHEAT/BREAKDOWN DUE TO LACK OF WATER/COOLANT CIRCULATION. FORD ANSWER: REPLACE WATER PUMP WITH UPGRADED WATER PUMP, FLUSH SYSTEM WITH ANTI-RUST CHEMICALS, REPLACE FREEZE PLUGS, REPLACE HEATER CORE, HOSES, THERMOSTAT AND REFILL WITH ANTI-FREEZE COOLANT AT A COST OF @ $1700.00. THIS VEHICLE HAS HAD REGULAR MAINTENANCE ON IT SINCE I'VE OWN IT 10/1999, IE. OIL CHANGES @5000K MI., COOLANT FLUSH @1/YR., BRAKES & TIRES CHECK/SERVICE @5000K MI. I BELIEVE FORD KNOWS OF THIS PROBLEM OR THEY WOULDN'T HAVE UPGRADED THE WATER PUMP TO CORRECT THE PROBLEM. AND I BELIEVE FORD SHOULD TAKE CARE OF THE REPLACEMENT OF THIS DEFECTIVE PART AND RELATED COMPONENTS. *NM
SMOKE WAS RISING FROM UNDERNEATH CAR ON THE RIGHT SIDE. TURNED ENGINE OFF AND FOUND OIL WAS RUNNING DOWN AND HITTING THE HOT EXHAUST PIPE CAUSING THE SMOKE. CAR WAS TOWED TO THE REPAIR FACILITY. REPAIR FACILITY FOUND THE OIL PAN GASKET WAS BULGED OUT ON THE RIGHT SIDE ABOUT 3/4" THUS ALLOWING OIL TO RUN OUT OF THE OIL PAN. OIL PAN GASKET WAS REPLACED. *JB
1998 FORD TAURUS ENGINE FAILED. *TS THE VEHICLES ENGINE FAILED WHILE ON AN EXIT RAMP. AS A RESULT THE VEHICLE RAN OFF THE LEFT SIDE OF THE ROAD AND STRUCK FOUR HIGHWAY SIGNS AND POLES. THE VEHICLE LEFT REAR DOOR, LEFT REAR QUARTER PANEL, LEFT REAR BUMPER AND RIGHT SIDE RUNNING PANEL WERE DAMAGED. *NM
TL*THE CONTACT OWNS A 1998 FORD TAURUS. WHILE DRIVING APPROXIMATELY 25 MPH ON NORMAL ROAD CONDITIONS, THE DRIVER HEARD A GUSHING NOISE OUTSIDE OF THE VEHICLE. THE VEHICLE WAS PULLED OVER TO THE SIDE OF THE ROAD AND OIL WAS OBSERVED LEAKING FROM UNDERNEATH THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC, WHO STATED THAT THE FAILURE WAS CONTRIBUTED TO THE ENGINE OIL PAN GASKET. THE OIL PAN GASKET WAS REPLACED AT THAT TIME. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC ON TWO SEPARATE OCCASIONS FOR IDENTICAL FAILURES. CURRENTLY, THE VEHICLE IS IN THE PROCESS OF BEING REPAIRED. THE FAILURE MILEAGE WAS BETWEEN 42,000-44,000 AND CURRENT MILEAGE WAS 110,000.
THE CAR HAS BEEN LOOKED AT THE GEARS SLIPPED OFF THE CAM, CAR COMPLETELY DIED
STUCK THERMOSTAT CAUSED A BOIL OVER. A FEW MONTHS LATER THE INTEGRATED PRESSURE/OVERFLOW BOTTLE CRACKED AND CAUSED A MAJOR LOSS OF COOLANT. THIS ALSO LEAD TO THE HEATER CORE BECOMING BLOCKED DUE TO THE LOSS OF COOLANT. UPDATED 12/07/07 *JB
THERE WERE PARTICLES COMING THROUGH THE AIR VENTS AND ALL OVER THE CAR. THE CONSUMER'S CHILDREN HAVE BECOME SICK AND THE CONSUMER WEARS A MASK. THE CONSUMER HAS TAKEN THE VEHICLE TO THE DEALER FOR REPAIR WITH NO SOLUTION. *JB
MY WHOLE COOLING SYSTEM HAS BECOME CORRODED BY THE COATING INSIDE OF THE HOSES THAT IS USED. I HAVE HAD MY HEATER CORE REPLACE 2 YEARS AGO AND MY RADIATOR FLUSHED. AND NOW IT IS FAILING AGAIN. A SERVICE BULLETIN HAS BEEN ISSUED, SO FORD KNOWS ABOUT THE PROBLEM. WHY AM I LEFT HOLDING THE BAG FOR REPAIRS ON DEFECTIVE PARTS. *NM
ENGINE COOLANT RESERVOIR SPRANG A LEAK ON THE BOTTOM SIDE. THERE IS ABOUT A 1-INCH GAP BETWEEN THE BOTTOM OF THE BOTTLE AND THE FENDER SO RUBBING AGAINST SOMETHING WAS NOT THE CAUSE. I CALLED A PARTS HOUSE WHO SAID THEY HAD REPLACED 3 OF THEM IN THE PAST 2 WEEKS. SEEMS LIKE AN ODD COINCIDENCE THE BOTTLES LEAK. I'VE NEVER SEEN ONE LEAK ON ANY CAR I'VE EVER OWNED.*AK
HEAD GASKET AND HEAD HAD TO BE REPLACED DUE TO OVERHEATING, TOTAL COST OF JOB WAS 1400. DOLLARS
WHILE DRIVING CONSUMER HEARD A LOUD NOISE WHICH WAS COMING FROM THE ENGINE. DEALER NOTIFIED.*AK
LAST SUMMER, MY 1998 FORD TAURUS BLEW AN ENGINE. IT WAS ABOUT 4000 MILES OVER WARRANTY. THE GARAGE TOLD ME THAT IT WAS NOTHING THAT I HAD DONE. THE PROBLEM WAS PROBABLY' A FAILURE IN THE OIL PUMP, THAT MY CAR HAD EXPERIENCED OIL PRESSURE PROBLEMS. THEY ALSO SAID THAT THEY REGRETTED THAT MY WARRANTY HAD EXPIRED. I HAD TO PAY TO REPLACE A NEW ENGINE. THEY SENT IN A REBUILT ENGINE, REPLACED THE BAD ENGINE, AND EXTENDED THE WARRANTY TO 100,000 MILES. THEN, THIS JULY (JULY 25,2003) I WAS DRIVING THE SAME 1998 FORD TAURUS WITH THE PREVIOUSLY BLOWN ENGINE. THE ADD COOLANT LIGHT CAME ON. I IMMEDIATELY STOPPED THE CAR. WATER WAS POURING FROM EITHER THE RADIATOR OR HOSE. I CALLED A TOW TRUCK AND HAD THE CAR TOWED HOME (ABOUT A DISTANCE OF 60 MILES). I HAD IT TOWED TO MY LOCAL MECHANIC. ON MONDAY MORNING, THE MECHANIC CALLED AND SAID THAT I HAD MANY MORE PROBLEMS THAT JUST A LEAK. HE SAID IT LOOKED LIKE I HAD A BLOWN HEAD GASKET. HE COULD NOT EVEN GET THE CAR TO START. BECAUSE THE CAR WAS STILL UNDER WARRANTY, I HAD IT TOWED TO THE BOWLING GREEN LINCOLN & MERCURY IN BOWLING GREEN OH. THIS IS WHERE I HAD ORIGINALLY PURCHASED THE CAR AND THE PLACE THAT HAD REPLACED THE ENGINE THE PREVIOUS SUMMER. AFTER WAITING NEARING TWO WEEKS TO GET PERMISSION FROM DETROIT (?) TO FIX IT, AN INSPECTOR WAS SENT DOWN TO EXAMINE THE DAMAGE. HIS REPORT INDICATED THAT THE PROBLEM WAS NOT FROM A DEFECTIVE ENGINE, BUT FROM ENVIRONMENTAL CONTAMINATION. THEY VOIDED THE WARRANTY. I ASKED WHAT ENVIRONMENTAL CONTAMINATION MEANT. I WAS INFORMED THAT THE INSPECTOR HAD DECIDED THAT MY CAR HAD BEEN IN A FLOOD. I WAS TAKEN BACK. MY CAR HAD NOT BEEN IN A FLOOD. THE MECHANICS, THE SERVICE REPRESENTATIVE, AND SERVICE MANAGER ALL CONFIRMED THAT THERE WAS ABSOLUTELY NO EVIDENCE THAT THE CAR WAS IN A FLOOD. I PERSONALLY HEARD THE SERVICE MANAGER TALK TO SOMEONE IN DETROIT CONFIRMING THAT THE CAR HAD NOT BEEN IN A FLOOD. DETROIT SENT OUT ANOTHER INSPECTOR WHO TOOK FLOOD SAMPLES FROM THE CAR.
1998 FORD TAURUS; 78000+ MILES: RECURRING TRANSMISSION PROBLEMS. OWNERS MANUAL INDICATES THAT THE ILLUMINATION OF THE CHECK ENGINE LIGHT MAY NOT BE REFERRING TO A MECHANICAL PROBLEM THAT WILL AFFECT PERFORMANCE OF THE VEHICLE. OUR LIGHT CAME ON ONE MONTH AFTER WE PURCHASED THE CAR. IT WOULD GO OFF WHEN WE CHANGED FLUIDS OR BRAND OF GASOLINE. ON JUNE 28TH THERE WAS A NOTICABLE CHANGE IN DRIVABILITY AS THE SPEEDOMETER STOPPED WORKING COMPLETELY AND THE CAR WOULD NO LONGER SHIFT FROM LOW GEAR. THE ENGINE WOULD REV TO 5000 RPMS TRYING TO SHIFT BUT COULD NOT. I CERTAINLY BELIEVE THIS TO BE A DANGEROUS SITUATION WHILE TRYING TO MANEUVER IN 55 TO 65 MPH TRAFFIC. AAMCO NOW TELLS ME THAT IT WILL COST 1500 T0 2000 DOLLARS TO FIX THE PROBLEM. I RAN A 1993 FORD VAN TO 270,000 MILES BUT I DID NOT KNOW THAT THIS MODEL HAD A 12 YEAR HISTORY OF SEVERE TRANSMISSION PROBLEMS. *AK
SMOKE BEGAN COMING OUT OF VENTS WHEN AIR CONDITIONING WAS TURNED ON. IF I TURNED IT OFF AND WAITED A FEW MINUTES, THE AIR CONDITIONING WOULD WORK AGAIN. THIS HAPPENED EVERY TIME I TRIED TO USE THE AIR CONDITIONING. IN SEPTEMBER, WHEN I TRIED USING THE HEATER, IT DID NOT WORK. I CHANGED THE THERMOSTAT AND HAD ENGINE COOLING SYSTEM FLUSHED. HOWEVER THIS STILL DID NOT RESOLVE MY PROBLEM. I CONTACTED MY LOCAL FORD DEALERSHIP,. THEY INFORMED ME THAT THIS A COMMON PROBLEM WITH THE 98 TAURUS. THE ENGINE COOLANT FORD MAKES YOU USE CLOGS THE SYSTEM AND TURNS THE COOLANT INTO SLUDGE. THE ONLY THING YOU CAN DO IS TO REPLACE THE HEATER CORE. THEY ALSO STATED THAT ON AVERAGE I WILL HAVE TO REPLACE THE HEATER CORE EVERY OTHER YEAR. THIS IS UNACCEPTABLE. *LA
POSSIBLE CAM FAILURE RESULTING IN TOTAL ENGINE LOST IF NOT FOR ALL FOUR CAMSHAFTS WELDED THIS DAY FOR THE COST OF $600. *LA
Showing 1–20 of 50 complaints
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on May 4, 2026