NHTSA Owner Complaint Log
This page lists owner-reported complaints filed with NHTSA for the 2014 Kia Forte. Complaints are unverified consumer reports submitted to NHTSA and do not by themselves prove a defect or defect rate.
DROVE OVER TRAIN TRACKS AT 15 MPH AND FELT IT BREAK. AT STOP, STEERING WHEEL HAS PLAY WHEN TURNED LIGHTLY. KNOCKS LOUDLY WHEN GOING OVER BUMPS AND TURNING. PART CAN CAUSE STEERING TO LOCK UP AT ANY MOMENT WHILE TURNING AND VERY UNSAFE. $13 PART, $200 LABOR
HEADLIGHTS AND INTERIOR LIGHTS FLICKERING/GOING OUT WHILE THE CAR IS IN MOTION OR STATIONARY ON CITY STREETS AND HIGHWAYS. SOMETIMES THEY DON'T COME BACK ON UNLESS I TINKER WITH THE HEADLIGHT CONTROL SWITCH. IT IS A MAJOR SAFETY CONCERN SEEING AS HOW I DRIVE DAILY IN THE DARK TO WORK
IN OCTOBER 2019 I BEGAN EXPERIENCING ENGINE ISSUES AND ON 11/16/19 I HAD A CATASTROPHIC FAILURE OF THE ENGINE OF MY 5 DOOR 2014 KIA FORTE AT NIGHT IN THE MIDDLE OF A BUSY ROAD FM528 IN FRIENDSWOOD, TEXAS. I HAD TO TOW THE VEHICLE 3 TIMES AT THE COST OF APPROX. $80 PER TOW AND SPENT AN ADDITIONAL $186 TO HAVE IT EVALUATED BY A MECHANIC. WE RESEARCHED THE ISSUE ONLINE AND DISCOVERED A NUMBER OF VEHICLES OF THE SAME MAKE AND MODEL HAVE BEEN EXPERIENCING "PISTON FLAP" WHICH IS A MANUFACTURING DEFECT OF THE CYLINDERS. EVEN THOUGH MY ENGINE IS WARRANTED FOR 100K MILES AND THE MILEAGE WAS AT 88K, KIA MOTORS REFUSED TO COVER THE ADDITIONAL TOWING EXPENSE TO GET IT BACK TO THE DEALERSHIP (GAY FAMILY KIA IN DICKINSON, TX) FOR INSPECTION. I HAVE BEEN WITHOUT MY PRIMARY TRANSPORTATION SINCE THAT TIME. TODAY, 1/7/2020 THE DEALERSHIP SAID THE ENGINE WOULD BE "REPAIRED" NOT COMPLETELY REPLACED. DURING THIS ENTIRE TIME KIA DENIED ME A LOANER CAR. AS A SINGLE MOM, (WHICH DEALERSHIP WAS AWARE) WE HAD TO TAKE MY COLLEGE STUDENT SON'S 1999 TRUCK TO VISIT MY FAMILY 2 HOURS AWAY AND IT HAD AN ALTERNATOR FAILURE AND HAD AN ADDITIONAL TOW BECAUSE OF NO LOANER CAR. ON 12/27 I HAD KNEE SURGERY AND THE ONLY VEHICLE I HAD TO DRIVE WAS A 1997 MIATA THAT WAS A STANDARD. I COULD NOT DRIVE THE STANDARD DUE TO MY SURGERY AND MISSED AN ADDITIONAL 2 DAYS OF WORK. THIS ISSUE IS DANGEROUS AND PUTS CONSUMERS AT GREAT RISK OF INJURY AND CRASH ON PUBLIC ROADS. KIA HAS DONE EVERYTHING IN THEIR POWER TO CIRCUMVENT AN ACCEPTABLE REMEDY TO THE SITUATION SO I AM NOW TURNING TO NHTSA FOR ASSISTANCE. PLEASE HELP! WILL PROVIDE WRITTEN REPORTS WHEN KIA DECIDES TO GIVE THEM TO ME. I STRONGLY DISAGREE WITH THE SIMPLE REPLACEMENT OF PARTS THAT WILL OBVIOUSLY FAIL ONCE THE VEHICLE PASSES 100K IN MILEAGE.
WE BUY THIS CAR IN 2 MONTHS AGO AND NOW THE ENGINE IS IN BAD CONDITION
CAR HAD BEGAN BURNING THROUGH OIL RAPIDLY BUT UPON INSPECTION AT OIL CHANGES, NO LEAK OR CAUSE COULD BE DETECTED. THE OIL LIGHT INDICATOR NEVER CAME ON EITHER. THE CAR WOULD BEGIN TICKING WHILE DRIVING, AND NOTICEABLY DROVE DIFFERENTLY BUT PROBLEM COULD NOT BE DETERMINED. NO CHECK ENGINE LIGHT EVER CAME ON. ON A CLEAR DAY WHILE DRIVING ABOUT 45 MPH ON HIGHWAY, VEHICLE GAVE A LOUD AND FORCEFUL JERK AND POPPING SOUND, AND PROMPTLY LOST POWER AND SPEED, AND THE BRAKES QUIT WORKING. I WAS FORTUNATE TO PULL OFF AND USE EBRAKE TO STOP CAR ONCE COASTED TO A SAFER SPOT. I COULD HAVE BEEN REAR ENDED. THE CAR HAD ONCE AGAIN BURNED THROUGH ALL OIL WITH NO INDICATION FROM THE PANEL, AND I WAS TOLD THE ENGINE HAD BLOWN. APPARENTLY THIS IS A VERY COMMON PROBLEM WITH THESE VEHICLES, THIS MAKE AND MODEL, WITH NO RECALL BEING DONE; HOWEVER, THERE IS A CLASS ACTION LAWSUIT BECAUSE OF SAME ISSUE WITH THIS ENGINE IN OTHER KIA MODELS.
TWICE WHILE DRIVING IN THE COUNTRY AT NIGHT ON A 2-LANE FM ROAD, THE HEADLIGHTS WENT COMPLETELY OUT WHEN CHANGING FROM LOW BEAM TO HIGH BEAM, AND ONCE,THEY WENT COMPLETELY OUT WHEN USING THE TURN SIGNAL. THEY CAME BACK ON IN A FEW SECONDS EACH TIME BUT THOSE FEW SECONDS WERE VERY DANGEROUS. *TR
Airbags failed to deploy after rear end collision.
I HAVE A KIA FORTE EX GDI PURCHASED USED FROM CAR MAX OF WHITEMARSH, MARYLAND. WHEN I STARTED THE VEHICLE, ON SEPTEMBER 22, 2019, THERE WAS A VERY LOUD TICKING NOISE. I ALLOWED THE CAR TO WARM UP. AS I DROVE AND REACHED 30MPH, ON CITY STREET, THE NOISE GREW LOUDER. WHEN I CHECKED THE OIL STICK IT WAS DRY. I GET REGULAR OIL CHANGES AND AM NOT DUE FOR ANOTHER ONE UNTIL MY CAR REACHED 84,319 MILES. MY CAR HAS EXACTLY 81,6000 MILES ON IT TODAY (SEPTEMBER 30, 2019 OR 2/13/2020 WHICH EVER COMES FIRST). MY CHECK OIL LIGHT OR ENGINE LIGHT NEVER CAME ON TO INDICATE MY OIL WAS EXTREMELY LOW. I PURCHASED OIL AND FILLED UP MY CAR. THE NOISE IS SOFTER NOW BUT IS STILL THERE. I RECEIVED A RECALL NOTICE FOR AN ISSUE DEALING WITH SOMETHING THAT MAY KEEP THE CAR FROM PASSING EMISSION TEST. I HAVE AN APPOINTMENT AT BOB BELL KIA (WHO ALWAYS SERVICES MY VEHICLE) IN ESSEX MARYLAND ON OCTOBER 17TH, 2019, TO CORRECT THAT ISSUE. I NOTIFIED THEM OF THE NOICE AND LACK OF OIL WITH NO INDICATION OF SUCH FROM THE CARS DASHBOARD. THEY WILL CHECK IT OUT ON THE 17TH WHEN I BRING THE CAR IN FOR THE RECALL ISSUE. AFTER READING SOME COMPLAINTS FROM OTHER OWNERS OF THE SAME VEHICLE I HAVE, I WILL NOT BE SURPRISED IF THEY TELL ME I NEED A NEW ENGINE. I STILL OWE $11,107.64 ON THE CAR AND WILL NOT BE DRIVING MY VEHICLE ANYMORE UNTIL THE MECHANIC CAN PINPOINT THE PROBLEM. WITH ALL THE COMPLAINTS OF FAULTY ENGINES AND FIRE HAZARDS WHY IS THE 2014 KIA FORTE EX GDI NOT INCLUDED IN AN ENGINE RECALL OR THE CLASS ACTION SUIT THAT IS ALREADY AGAINST KIA FOR THE SAME EXACT ISSUES IN THEIR SORENTO AND OTHER MODELS? WHO CAN I TURN TO FOR HELP WITH THIS ISSUE SINCE I HAVE A VEHICLE I CAN NOT SAFELY DRIVE BUT STILL MUST PAY ON?
I WOKE UP ONE DAY AND WENT TO HEAD OVER TO MY BUDDIES HOUSE. IT WAS A FIFTEEN MINUTE DRIVE AND WHEN I GOT THERE I TOLD HIM MY CAR STARTED SOUNDING FUNNY ON THE WAY OVER. THE OIL WAS GOOD AND EVERYTHING ELSE SO WE TOOK IT FOR A DRIVE DOWN THE STREET SO HE COULD LISTEN TO IT. WE GOT TO THE LIGHT A HALF MILE DOWN THE HOUSE AND THE ENGINE MADE A SCRATCHING NOISE AND I STARTED TO LOSE POWER I ALSO FELT MY STEERING WHEEL LOSE POWER STEERING AND THEN I WAS AT THE FRONT OF THE ROW IN THE TURN LANE. MY CAR CRAWLED THROUGH THE INTERSECTION BUT I MADE IT TO THE SIDE OF THE STREET AND MY PARENTS TOWED IT HOME ON THEIR TRAILER. WE TOOK IT TO AN AUTO SHOP AND THE MECHANIC SAID THE ENGINE FAILED DUE TO CHEAP STOCK BEARINGS AROUND THE CAM. THE BEARINGS GAVE OUT AND THE METAL SHREDDED INSIDE AND WAS SENT THROUGH THE ENGINE. SINCE IT'S PRE OWNED I CAN'T GET A NEW ENGINE AND THIS SPECIFIC ENGINE IN THIS MAKE AND MODEL HASN'T BEEN RECALLED YET.
MY 2014 KIA FORTE SUDDENLY STARTED MAKING A KNOCKING SOUND AND SHUT OFF WHILE DRIVING DOWN THE INTERSTATE. AFTER TOWING VEHICLE TO THE SHOP I WAS TOLD THAT THE ENGINE NEEDS TO BE REPLACED. THE MECHANIC TOLD ME HE DOES NOT UNDERSTAND WHY AS THERE WAS NOT ANYTHING THAT COULD HAVE CAUSED THIS. ARE FLUIDS WERE GOOD AND CLEAN. UPON REVIEWING KIA HAD PROBLEMS WITH THIS ENGINE IN OTHER VEHICLES WHICH LED TO RECALLS.
KNOCKING SOUND AND ENGINE BLEW WITH UNDER 58,000 MILES. BOUGHT MY CAR BRAND NEW JUST OVER 5 YEARS AGO.
BOUGHT VEHICLENUSED FROM PRIVATE PARTY. RAN GOOD LOOKS GREAT DROVE 500 MILES ENGINE STARTED MAKING A KNOCKING SOUND AND SHUT OFF SMOKE FROM UNDER HOOD. OPENS HOOD AND SAW/SMELLED BURNING UNDER ENGINE COVER, PULLED COVER AND SAW MELTED WIRES AND MELTED PLASTIC. ENGINE WAS LOCKED UP. TOWED TO LOCAL GARAGE AND WAS DETERMINED ENGINE OUT A ROD THROUGH THE BLOCK AND SOMETHING WAS DEFINITELY BURNING KN TOP AT 1 POI T. EMAILED KIA GOT A CASE # BUT HAVE BEEN PLACED ON HOLD FOR OVER 30 MIN PROB LONGER COULDNT WAIT AT LEAST 3 DIFFERENT TIMES. DEALER WAS NO HELP AND SAID I NEEDED TO CONTACT KIA CORPORATE. SUCH A SHAME! 89,565 MILES AND I HAVE A BROKEN VEHICLE.
WHILE DRIVING AT NIGHT, MY HEADLIGHTS WOULD GO COMPLETELY OUT. ONCE I SWITCH THEM ON AGAIN, THEY WOULD GO OUT ONCE AGAIN. THIS WOULD TAKE PLACE EVERY COUPLE OF MINUTES AND IS VERY DANGEROUS. I TOOK MY CAR INTO THE DEALERSHIP AND WAS TOLD THAT THEY KNEW EXACTLY THE ISSUE BECAUSE THEY REPAIRED QUITE A FEW CARS WITH THE SAME ISSUE. THE TOTAL COST TO REPAIR THIS ISSUE WAS $238. THIS IS VERY DANGEROUS AND SHOULD BE PLACED ON THE RECALL LIST.
WHILE DRIVING ON THE FREEWAY, ENGINE DIED AND THEN RESTARTED. THE CAR ENGINE STARTED TO MAKE A LOUD NOISE AND IT WOULD NO LONGER SHIFT, SO MANUALLY SHIFTED AND THE ENGINE TEMP GAUGE BEGAN TO RISE SO, PULLED OVER AND SHUT THE ENGINE OFF AND CALLED AAA TO TOW THE CAR TO A DEALER. KIA DEALER ADVISED THAT CYLINDER 3 ROD BEARING FAILURE OCCURRED WHICH SUCKED ALL THE OIL INTO THE ENGINE (THEY SAID THAT IS HOW THEY IMMEDIATELY KNEW WHAT THE ISSUE WAS). WE JUST BOUGHT THIS CAR 6 WEEKS EARLIER, BUT I COULD NOT AFFORD THE EXTENDED WARRANTY. WEI HAD A TUNE UP AND OIL CHANGE 2 WEEKS EARLIER AND WE FAITHFULLY CHECK THE OIL TO ENSURE IT IS AS EXPECTED. THE DEALER ADVISED THERE WAS NO WAY WE COULD HAVE AVOIDED THE ENGINE FAILURE, AND WE NEEDED A NEW ENGINE. THE COSTS WAS $5,111.96 TO REPLACE. WE CANNOT AFFORD TO GET RID OF THE VEHICLE AND I WAS FORCED TO REPLACE THE ENGINE. NOW WE HAVING OVER $12,000 BETWEEN BUYING IT AND FIXING IT. FAILURE ON A FREEWAY IS UNACCEPTABLE, ESPECIALLY DURING RUSH HOUR. KIA NEEDS TO DO SOMETHING ABOUT THESE ENGINES AS THIS SHOULD NEVER HAVE HAPPENED. MAYBE IF ENOUGH PEOPLE REPORT THESE ISSUES, THEY WILL BE FORCED TO FIX THE PROBLEM AND REIMBURSE PEOPLE LIKE US THAT CANNOT AFFORD THESE KIND OF PROBLEMS.
WHILE DRIVING DOWN THE STREET, HEARD A RASPING NOISE COMING FROM THE STEERING WHEEL AND THEN NOTICED THE AIR BAG LIGHT CAME ON AND STAYED ON.
MY VEHICLE WAS SOLD TO ME UNDER A WARRANTY. UPON DRIVING THE ENGINE LOST ALL POWER. WOULD NOT RESTART. ENGINE HAS BEEN REPLACED TWICE BY KIA. AS WELL AS A REPLACEMENT OIL PAN RANDOMLY. MY LONG TIME MECHANIC SAID THE OIL PAN WASN'T NEEDED TO BE REPLACED. 1ST REPLACEMENT ENGINE WAS DEFECTIVE. IN TOTAL THE CAR HAS HAD 3 ENGINES. EMISSIONS PROBLEM EVER SINCE. LIGHT ON AND KIA HAS BILLED AND USED ALL OF THE WARRANTY COVERAGE. ALL DOCUMENTATION PROVIDABLE. ALL OIL CHANGES PROVIDABLE.
THE AIRBAG LIGHT TURNS ON AND OFF INTERMITTENTLY, USUALLY TURNING ON AFTER STARTING THE CAR AND REACHING SPEEDS ABOVE 15MPH. IF I STAY AROUND 20MPH OR BELOW, IT WILL TURN OFF, BUT IF I INCREASE SPEED IT WILL TURN BACK ON. IF I STOP, TURN, OR SLOW DOWN, THE LIGHT MAY TURN ON OR OFF; IT IS RANDOM. THE CAR WAS NOT INVOLVED IN AN ACCIDENT WHEN THE ISSUE WITH STARTED. IT APPEARS THERE HAS BEEN A RECALL FOR SIMILAR ISSUES FOR THE 2010-2013 KIA FORTE. THE 2014 SHOULD BE INCLUDED AS WELL.
ON 08-05-2019 I WAS TRAVELING ONTO THE INTERSTATE, UPON ACCELERATION MY AUTOMOBILE BEGIN TO POWER DOWN, IN FRONT OF A TRACTOR TRAILER. I ATTEMPTED TO MOVE OVER TO THE RIGHT SHOULDER BUT THE CAR WOULDN'T ACCELERATE TO DO SO IN A SAFE MANNER. AFTER ABOUT ONE MINUTE OF CONTINUOUSLY ACCELERATION, THE CAR BEGIN TO MOVE. I HAVE BROUGHT THIS TO THE ATTENTION OF KIA IN THE PAST, THE CAR HAS BEEN TAKEN TO SEVERAL KIA DEALERSHIP WITH NO RESOLUTION. THIS REMAINS TO BE AN EXTREME SAFETY CONCERN, THAT COULD BECOME DEADLY. ON 08-03-2019, IN AN UNRELATED INCIDENT I WITNESSED A KIA SOUL BURN TO THE GROUND AFTER CATCHING FIRE; SIMPLY PUT THESE VEHICLES APPEAR TO BE VERY UNSAFE FOR OPERATION.
CAR CONSUMING OIL WITHIN SHORT TIMEFRAME. NO LEAKS AND HAVE TO ADD A QUART EVERY FEW DAYS. CAR IS NOW COMPLETELY UNDRIVEABLE, CAR STOPPED ACCELERATING ABOUT 2 MONTHS AGO AND NO CODES ARE FLASHING AND NO CHECK ENGINE LIGHT. CAR HESITATES TO ACCELERATE AND IS VERY NOISY. REPLACED SPARK PLUGS AND COIL PACK AND PROBLEM PERSISTS, THIS CAR IS NOW UNSAFE TO DRIVE BECAUSE IT WILL NOT ACCELERATE AND CONSUMES UNHEALTHY AMOUNTS OF OIL.
PURCHASED ON JUNE 27 2019. 3 WEEKS LATER I STOPPED BY DEALERSHIP FOR ASSISTANCE IT'S BEEN A NIGHTMARE SINCE. CAR HAD BEEN CONSUMING OIL AND I'VE SPENT THOUSANDS OF DOLLARS FOR REPAIRS. JUST HAD MASTER MECHANIC REPLACING CATALYTIC CONVERTER AND IT'S ALREADY PLUGGED. KAY ON BOTH ACCOUNTS ASSURED ME NOTHING WRONG, NICE CAR HAS 23 BRAINS IT'S THE ECHO DRIVE. ENGINE LIGHT BLINKS AND NO ONE CAN GET A CODE READING, NO ONE BUT KIA. BOTH SERVICE REP, TYLER AND KIA CONSUMER AFFAIRS AGENT, DEAN THOUGHT I WAS, AND REFERRED TO ME AS WHARTON WHOM PURCHASED THE CAR 2014 AND HAD ENGINE PROBLEMS ACCORDING TO THESE INDIVIDUAL THAT THOUGHT I WAS THERE FOR SAME REASON. DEAN FROM KIA CONSUMER AFFAIRS SPECIFICALLY TOLD ME DURING A PHONE CONVERSATION DEC 2020, AND VERIFYING MY VIN NUMBER THAT MY VERTICAL WAS IN FACT ON RECALL LIST. I CALL JAN 20TH 2021 AND TOLD I WAS NOT AND CASE WAS CLOSED DUE TO I BEING INFORMED OF RECALL TO WHICH I CALLED AFTER SEEING ARRIVAL ON LINE. I'M ADVISED TO GO ON YOUR WEBSITE WITH MY VIN NUMBER AND FIND OUT IF I'M PART OF RECALL. I AM NOT. WHY????. THIS CAR OBVIOUSLY IS DEFECTIVE IF I'M THOUGHT TO BE SHANNON TRYING TO TAKE KIA FOR A RIDE AND I'M THE 3RD OWNER WITH SAME PROBLEM AS PRIOR OWNERS. THIS CAR IS NOT SAFE. I'VE TURNED TO KIA TO BEGIN WITH AND PAID FOR COMPRESSION TESTS, REPLACED CATALYTIC CONVERTER OVER 1000.00 DOLLARS AND IT NEEDS REPLACING AGAIN DUE TO OIL CONSUMPTION. FACT IS I WAS SOLD A CAR WITH ENGINE PROBLEMS AND HAVE ALMOST BEEN REAR END DUE TO POWER LOSS, LIMP MODE TYLER CALLED IT... IT'S NOT SAFE. WHAT CAN I DO NOW I KNOW I'M OUT 9000.00 DOLLARS ON THIS CAR ON MY SSDI PAY. MUCH MORE DETAILS DOCUMENTED WHO WHAT WHEN HERE AND WHAT WAS SAID. TIMES AND DATES FOR ENTIRE DURATION OF EVENTS STARTING WITH KIRA AT RON BOUCHARDS IN FITCHBURG MASS JULY OF 2019 AND OCT 2020.*DT CONSUMER STATED SHE WOULD LIKE THE COMPLAINT TO BE REMOVED FROM PUBLIC VIEWING.*JB*DT CONSUMER STATED KIA HAS NO RECALL ON THE VEHICLE EVEN THOUGH OIL LEAK IS RECALLED AND WILL NOT MAKE A RECALL APPOINTMENT.*JB
SRS AIRBAG LIGHT STARTED LUMINATING INTERMITTENTLY. DISCONNECTED AND RECONNECTED CABLES UNDER PASSENGER SIDE SEAT AND AIRBAG LIGHT WENT OFF. WITHIN 2 DAYS THE AIRBAG LIGHT IS BACK ON. THE CAR WAS NOT INVOLVED IN A CAR ACCIDENT. TOOK IT TO THE DEALERSHIP FOR DIAGNOSTICS. THERE APPARENTLY WAS A RECALL FOR THIS ISSUE BUT IT IS FOR 2010-2013 KIA FORTE. DEALER WAS NOT YET ABLE TO ACTUALLY TELL ME THE ISSUE CAUSING THE AIRBAG LIGHT TO REMAIN ON. STILL A MYSTERY.
ON JULY 17,2019 MY KIA FORTE 2014 STOP ON I-75 NORTHBOUND IN PERRY, GA WITH A 18 WHEELER ON MY TAIL @80MPH. I HAD NO POWER IT JUST CUT OFF. THIS WAS AFTER A OIL CHANGE @ WALMART IN CORDELE, GA 13 DAYS EARLIER THERE WAS NO OIL AND IT HAD RUN OUT FROM THE FILTER. BOTH ASE CERTIFIED MECHANIC @ HUTCHINSON KIA AND AN INDEPENDENT CERTIFIED MECHANIC. DEALER COULDN'T DETERMINE LEAKAGE,SECOND SOUND THE ENGINE WAS CRACKED CAUSED PROBLEM. IT WAS A DANGEROUS SITUATION FOR MY DAUGHTER HER LIFE WAS IN DANGER IN FAST HIGH VOLUME INTERSTATE TRAFFIC. THE ENGINE HAS A DEFICIENCY IN THESE GDI ENGINES,SHOULD RECALLED. I WAS TOLD BY A RELIABLE SOUCE THAT BOTH THE KIA'S AND THEIR SISTER COMPANY SHARE THE SAME ENGINE AND THERE HAVE BEEN PROBLEMS WITH BOTH ENGINE TYPE GDI 2014 MODEL KIA FORTE AND OTHER MODELS WITH THIS KIND OF ENGINE.
THE CAR WILL STALL WHILE DRIVING DOWN THE ROAD. SUDDENLY. IT HESITATED AND THE CHECK ENGINE LIGHT KEEPS COMING IN DESPITE GOING TO SEVERAL MECHANICS. WHAT IS WRONG?!!!
I BOUGHT MY CAR IN 2013, HAD IT LESS THAN 6 YEARS. THE AIRBAG LIGHT IS ON AND REMAINS ON, THE CAR WAS NOT IN A CAR ACCIDENT WHEN THE AIR BAG LIGHT CAME ON. THE AIR BAG LIGHT AT FIRST CAME ON AND THEN WILL DISAPPEAR A COUPLE TIMES BUT NOW HAS REMAINED ON. I TOOK IT TO THE DEALERSHIP AND THERE IS A SHORT CIRCUIT IN THE AIRBAG CONTROL UNIT. THERE IS A RECALL FOR THIS ISSUE BUT IT IS FOR 2010-2013 KIA FORTE. I BELIEVE MY CAR SHOULD BE INCLUDED IN THIS RECALL.
2014 KIA FORTE: VEHICLE WILL BE STATIONARY, IN MOTION, OR TURNING AND THE AIRBAG LIGHT WILL TURN ON AND OFF RANDOMLY, IT HAS BEEN STAYING ON IN THE PAST FEW DAYS. DEALERSHIP STATED "AIRBAG NEEDS REPLACING, BECAUSE IN AN ACCIDENT AIRBAG WILL NOT DEPLOY" THIS CAR IS ONLY 5 YEARS OLD WITH ONE OWNER LESS THAN 75,000 MILES ON IT. SOMETHING IS NOT RIGHT WITH HOW THE AIRBAG WAS INSTALLED BY KIA MANUFACTURES.
CAR NEEDS OIL EVERY 1,000 MILES OR SO WITH NO LEAKS. ENGINE EATS OIL AND IS ALWAYS SEVERAL QUARTS LOW. DAUGHTER WAS DRIVING CAR AND IT STOPPED EXCELLERATING. CATALYTIC CONVERTER JUST HAD TO BE REPLACED AT 82,000 MILES. ENGINE NOISE WITH VIBRATIONS. MY DAUGHER IS AFRAID TO DRIVE THE CAR. KIA SAYS WARRANTY EXPIRED 2,000 MILES AGO AND WON'T FIX CAR. CAR IS EXTREMELY UNSAFE!
TL* THE CONTACT OWNS 2014 KIA FORTE. THE CONTACT STATED THAT UPON RE-ENTERING THE VEHICLE WITH A PASSENGER, THE VEHICLE WAS STARTED AND SMOKE EMITTED FROM THE CHARGER PORT. THE CONTACT HAD TO PULL OF THE ROAD AND TURN OFF THE VEHICLE AS THE FLAMES ERUPTED WHICH CAUSED THE DRIVER AND FRONT PASSENGER TO HAVE TO EXIT THE VEHICLE. THE FIRE WAS COMING THROUGH THE LIGHTER/CHARGER PORT CONNECTION. THE VEHICLE WAS DESTROYED DUE TO THE FAILURE. A FIRE INSPECTION REPORT WAS PROVIDED AFTER THE FLAMES HAD BEEN EXTINGUISHED. A DEALER WAS CONTACTED CRAIN HYUNDAI OF NORTH LITTLE ROCK, 5660 WARDEN RD, NORTH LITTLE ROCK, AR 72116, (501) 232-4018 BUT HAD NOT PROVIDED ANY TECHNICAL GUIDANCE AS OF YET. THE VIN WAS NOT AVAILABLE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE TO DETERMINE IF THEY MAY INVESTIGATE THE FIRE. 100,000.
STEERING: STEERING MAKES A LOUD KNOCKING NOISE UNDER THE DASHBOARD WHEN TURNING THE WHEEL LEFT OR RIGHT. NOISE HAPPENS WHEN VEHICLE IS STATIONARY OR MOVING AT ANY SPEED. KIA HAS RECALLED SOME 2014-2016 SOULS WITH THE SAME PROBLEM BUT THEY HAVE NOT RECALLED THE FORTE. LIGHTING: HEADLIGHTS AND DASHBOARD LIGHTS GO OUT WHEN TURNING ON THE TURN SIGNALS.
THE STEERING WHEEL MECHANISM WILL MAKE A KNOCKING NOISE THAT IS FELT MORE THAN HEARD. IT SEEMS TO BE GETTING WORSE, AND IS MORE NOTICEABLE WHEN TURNING THE WHEEL WHILE STOPPED AS OPPOSED TO TURNING WHILE IN MOTION. RESEARCH HAS SHOWN THAT THIS IS A VERY COMMON PROBLEM AMONG SEVERAL MODELS OF KIA, ESPECIALLY IN THE SOUTHEAST. I TOOK IT TO A DEALER TODAY TO HAVE CHECKED AND WAS TOLD IT WAS THE FLEX COUPLER. THE RECEPTIONIST TOLD ME THEY GET A LOT OF THESE ALL THE TIME AND THAT THEY CAN BECOME VERY DANGEROUS IF NOT FIXED SOON. MY RESEARCH ALSO REVEALED THAT SOME MODELS HAVE BEEN AFFORDED EXTENDED WARRANTIES AND FREE REPLACEMENT, BUT OTHERS HAVE NOT EVEN THOUGH THE PROBLEM, SYMPTOM, AND SOLUTION ARE THE SAME. BTW, THE REPAIR BILL WAS OVER $400...ABOUT $2 FOR PART AND THE REST WAS LABOR, TAX AND MISC.
THIS HAPPENED BACK IN JUNE OF 2019. I LEFT WORK NORMALLY AND NOT EVEN 2 MINUTES DOWN THE ROAD, MY CAR STARTED STRUGGLING TO MOVE FORWARD. IT WAS BUCKING AND COULD NOT ACCELERATE, BUT STILL TRYING TO GO FORWARD. THEN SUDDENLY IT STARTED MAKING A VERY LOUD TAPPING NOISE, STILL BUCKING AND THEN A LARGE POP AND THE CAR STOPPED MOVING SINCE IT DIED IN THE MIDDLE OF THE ROAD. THIS ALL HAPPENED WITHIN A MATTER OF SECONDS. SMOKE STARTED SEEPING OUT OF THE HOOD OF MY CAR. I HAD NO LIGHTS ON IN MY CAR ON MY DASHBOARD. I ALWAYS HAD FREE REGULAR MAINTENANCE(OIL ETC.) DONE AT MY KIA DEALERSHIP. I OBVIOUSLY HAD TO HAVE IT TOWED AND GOT IT TO THE DEALERSHIP SO THEY COULD LOOK AT IT IN THE MORNING. THEY SAID THEY DIDN'T KNOW WHY, BUT MY ENTIRE ENGINE HAD JUST BLOWN OUT FOR NO REASON. MY CAR WAS ONLY AT 87,000 MILES AND IT WAS JUST TOTALLED. I WASN'T WORRIED INITIALLY BECAUSE I PAID EXTRA FOR THE WARRANTY TO FIX ANY MAJOR PROBLEMS LIKE THIS, HOWEVER I CAME TO FIND OUT THE WARRANTY REFUSED TO COVER THE ENTIRE COST TO REPLACE THE PRICE OF A NEW ENGINE IN MY VEHICLE AND ON TOP OF THAT, WHEN THE ENGINE BLEW IT KILLED THE COMPUTER IN MY CAR, AND THE DEALERSHIP ALSO STRONGLY ADVISED I REPLACED SEVERAL OTHER THINGS ON THE VEHICLE. I'D HAVE TO PULL OUT MY RECEIPTS TO GIVE YOU ALL AN EXACT AMOUNT BUT WE PAID AT LEAST $5,000 - $10,000 OUT OF POCKET FOR THE ENGINE AND COMPUTER ALONE. TODAY IS MAY 8TH, 2021, ALMOST 2 YEARS LATER AND I JUST HAPPENED TO BE ON KELLEY BLUE BOOK TRYING TO SEE WHAT I CAN SELL MY GARBAGE KIA FOR. I HAPPENED TO ENTER MY VIN INTO THE RECALL CHECKER AND I COULD NOT BELIEVE MY EYES, ENGINE RECALL ISSUED LATE 2020. I HAVE NOT BEEN NOTIFIED BY ANYBODY ABOUT THIS AND PROBABLY WOULD HAVE NEVER BEEN TOLD SEEMING AS THEY ALREADY BASICALLY STOLE MY MONEY FROM ME 2 YEARS AGO. I AM REALLY HOPING YOU CAN HELP ME RESOLVE THIS AND MORE THAN HAPPY TO PROVIDE ANYTHING YOU NEED.
SO AS I'M DRIVING, THE AIRBAG INDICATOR LIGHT COMES ON. IT'S STEADY ONE MINUTE AND THEN IT WILL GO OFF AND THEN IT WILL COME BACK ON. I HAVE NEVER BEEN IN ANY KIND OF ACCIDENT FOR IT TO DO THIS. IT CAME OUT OF NO WHERE.
2014 KIA FORTE EX 2.0 LITER GDI ENGINE HAS KNOCKING NOISES. WHEN I TOOK IT TO GROSSINGER KIA OF LINCOLNWOOD, IL THEY QUOTED OVER $4,300 + LABOR DUE TO METAL SHRAPNEL IN THE ENGINE AND THEY TOLD ME THAT I NEEDED TO REPLACE THE SHORT BLOCK OF THE ENGINE. THEY TOLD ME THAT THE CAR WAS OUT OF WARRANTY BECAUSE I WAS NOT THE FIRST OWNER AND THAT THE ENGINE WAS ONLY COVERED UNTIL 60,000 MILES. I BOUGHT THE CAR USED AROUND NOVEMBER 2018 WHEN IT HAD AROUND 61,000 MILES BECAUSE IT HAD A CLEAN CARFAX HISTORY BUT I NOTICED THE KNOCKING NOISES BECAME INCREASINGLY LOUDER UNTIL I TOOK IT TO THE DEALER. I'VE SEARCHED ONLINE AND IT APPEARS THAT HYUNDAI/KIA HAS A MANUFACTURING DEFECT WITH THEIR GDI ENGINES AS THERE ARE CURRENTLY LAWSUITS CONCERNING THEIR ENGINES FAILING DUE TO A MANUFACTURING DEFECT. I BELIEVE THIS CAR ALSO HAS A DEFECT ENGINE AND AN INVESTIGATION SHOULD BE DONE TO COMPEL THEM TO REPAIR THEIR DEFECTIVE ENGINES.
MY VEHICLES STEERING COUPLING PINGS AND SOUNDS LIKE IT'S COME LOOSE OR BROKEN. SAME ISSUE HAPPENED TO ANOTHER KIA IN THE FAMILY A 2012 KIA SOUL MY BROTHER IN LAW OWNS. THAT KIA HAD A RECALL FOR THE STEERING COUPLING, THE 2014 KIA FORTE DOES'NT HAVE THIS FOR A RECALL YET BY KIA. I CONTACTED KIA COMPLAINT #13202206 FOR RESOLUTION BUT NO RESOLUTION REC'D TO DATE 12/13/2019.
TL* THE CONTACT OWNS A 2014 KIA FORTE. WHILE DRIVING 25 MPH, THE CHECK ENGINE AND OIL WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS TAKEN TO GENE MESSER KIA (LOCATED AT 6006 19TH ST, LUBBOCK, TX 79407, (806) 776-5600) WHERE IT WAS DIAGNOSED THAT THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 70,000.
LAST WEEK MY AIR BAG INDICATOR LIGHT STARTED COMING ON. MY CAR HAS NOT BEEN INVOLVED IN ANY CRASH FOR A CRASH REPAIR TO BE A FACTOR. I WAS DRIVING WHEN THE LIGHT FIRST CAME ON. THE LIGHT DOES GO OFF WHEN IT WANTS TO. I HAVE TRIED RESETTING THE CAR BY DISCONNECTING THE BATTERY FOR A FEW MINUTES, THIS DID NOT HELP. I AM VERY SCARED THAT THE AIR BAGS COULD DEPLOY AT ANY GIVEN MOMENT. TODAY MY TRACTION CONTROL LIGHT ILLUMINATED AND WOULD ONLY GO OFF IF I RESTARTED THE CAR BUT LESS THAN A MILE THE LIGHT CAME BACK ON. AND BECAUSE THIS LIGHT WAS ON MY CRUISE CONTROL WOULD NOT SET.
TAKATA RECALL
IN JUNE OF 2019, I HAD TO REPLACE THE ENGINE IN MY 2014 KIA FORTE. MY MECHANIC SAID IT WAS DUE TO COMPLETE ENGINE FAILURE AND WHEN HE REMOVED THE OLD ENGINE METAL FRAGMENTS AND PIECES WERE FOUND IN THE OIL PAN WHERE THE ENGINE WAS LITERALLY FALLING APART. THIS COST ME A SIGNIFICANT AMOUNT OF MONEY TO REPLACE AND KIA WAS ABSOLUTELY UNWILLING TO HELP COVER ANY COSTS OF THE REPAIRS AND REPLACEMENT. THIS IS UNACCEPTABLE ON SO MANY LEVELS. I PURCHASED THE CAR FROM KIA IN 2014 AND WHEN I REPLACED THE ENGINE IN 2019 IT HAD 140,000 MILES ON IT. WHEN I WAS COMING BACK FROM MY SON'S BIRTHDAY OUTING, THE CAR MADE A REALLY LOUD NOISE AND WHEN I HIT THE GAS IT WOULD NOT GO. WE WERE ABLE TO PUT IT IN NEUTRAL AND MAKE IT TO THE NEAREST PULL OFF SPOT BUT HAD TO CALL A TOW TRUCK TO HAVE IT TOWED TO MECHANIC SHOP.
MY BRAKE LIGHTS STAY ON AT ALL TIMES WHILE CAR IS TURNED ON
EXCESS ENGINE WEAR MAY BE INDICATIVE OF OTHER MODELS THAT HAVE BEEN RECALLED, CAR IS UNDER 100,000 MILES AS OF TODAY. EXCESSIVE ENGINE KNOCK CAUSED CONCERN AND KIA CLAIMS IT NEEDS A NEW ENGINE, BUT I HAVE NOTICED QUITE A FEW OTHER MODELS ALL HAVE THE SAME ISSUE, JUST NOT INCLUDING THE FORTE YET. CAR KNOCKS BOTH SITTING STILL AND IN MOTION, KNOCKS FASTER DURING DRIVING.
THE AIRBAG LIGHT CAME ON, AND THE HORN AS WELL AS THE STEERING WHEEL BUTTONS HAVE ALL STOPPED WORKING. I WAS TOLD THAT A SPRING CLOCK NEEDS TO BE REPLACED SOMEWHERE BUT I BOUGHT THE CAR BRAND NEW AND ITS ONLY 6 YEARS OLD. ALSO MY CATALYTIC CONVERTER WENT OUT AND MY CAR IS BURNING FUEL AND OR OIL AND NO ONE CAN TELL ME WHY. I WASN'T DOING ANYTHING BUT A NORMAL DRIVE WHEN THESE ISSUES BEGAN TO OCCUR. HELP *TR
PLAY IN STEERING WHEEL ,WHEN LOOKING IT UP ,PROBLEM SEEMS COMMON FOR THE STEERING COUPLER TO GO OUT,CAUSES A JERK IN THE WHEEL AT TIMES WHILE DRIVING. SITTING STILL IT WILL HAVE ALOT OF PLAY MOVING LEFT AND RIGHT AND A NOISE. A EXTENDED WARRANTY HAS BEEN GIVEN FOR SOME MODELS EXCEPT MINE.
The contact owns a 2014 Kia Forte. The contact stated while driving 53 MPH at night, the vehicle started shuddering and then stalled. The check engine warning light illuminated. The contact veered to the side of the road. The contact was able to restart the vehicle; however, the vehicle was towed to the contact’s residence. The vehicle was then towed to the used car dealer where it was purchased. The used car dealer diagnosed that the catalytic converter was misfiring. The vehicle was repaired; however, the failure reoccurred while driving five months later. The vehicle was taken back to the used car dealer where it was diagnosed that the catalytic converter was misfiring. The vehicle was repaired; however, the failure persisted and the vehicle was taken back to the used car dealer three more times. The used car dealer provided the same diagnostic and repaired the vehicle; however, the failure persisted. The vehicle was not repaired. The local dealer was not notified of the failure. The manufacturer was not notified of the failure. The failure mileage was approximately 160,800.
TL* THE CONTACT OWNS A 2014 KIA FORTE. WHILE DRIVING, A TICKING NOISE WAS HEARD FROM THE ENGINE, AND THE VEHICLE HESITATED AND ALMOST STALLED TWICE. THE VEHICLE WAS TAKEN TO ALM KIA SOUTH (4310 JONESBORO RD, UNION CITY, GA 30291, (678) 827-8900) FOR AN OIL CHANGE. THE CONTACT WAS INFORMED THAT A NEW ENGINE WAS NEEDED BECAUSE OIL WAS BURNING IN THE ENGINE. THE VEHICLE WAS NOT REPAIRED. THE VEHICLE WAS LATER TAKEN TO AN INDEPENDENT MECHANIC WHO STATED THAT THE ENGINE WAS BURNING OIL. THE VEHICLE WAS TAKEN TO ANOTHER INDEPENDENT MECHANIC WHO STATED THAT THERE WAS NO OIL IN THE ENGINE. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 94,000.
TL* THE CONTACT OWNS A 2014 KIA FORTE. WHILE DRIVING VARIOUS SPEEDS, THE AIR BAG WARNING INDICATOR ILLUMINATED. THE DEALER AND MANUFACTURER WERE NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE MILEAGE WAS 81,000.
03/08/19 AT 5:45AM I WAS ENTERING US HWY 23 N. BOUND FROM CENTRAL AVE. IN SYLVANIA OHIO. THE CAR WAS HAVING ISSUES WITH ACCELERATION AS I TRIED TO GET ON THE FREEWAY. SUDDENLY I HEARD LIKE A FAN NOISE, THE OIL LIGHT CAME ON FOLLOWED BY THE ENGINE LIGHT AND THE CAR JUST SHUT OFF! I PULLED TO THE SIDE OF THE ROAD AS SMOKE WAS FILLING THE CABIN. I GOT OUT AND WENT AROUND FRONT AND FLAMES WERE COMING OUT BETWEEN THE HOOD AND THE FENDER ON THE PASSENGER SIDE. I CALLED 911. ONE POLICE AND 2 FIRE TRUCKS SHOWED UP IN NOTHING FLAT! THE FIRE WAS MOVING INTO THE CAB. THE CAR IS A TOTAL LOSS! AFTER MY OWN RESEARCH I FIRMLY BELIEVE IT WAS THE COOLING FAN RESISTOR. THAT WOULD EXPLAIN THE NOISE I HEARD AND THE FIRE.
WHEN CAR IS IN MOTION ON A DOWNWARD SLOPE LIKE ON A BRIDGE OR WHERE A ROAD IS BROKEN, ON APPLYING BRAKE IT SEEMS LIKE THE PEDAL IS TOUCHING THE GROUND MAKING GRINDING NOISE AND CAR SKIDS AND DOESN'T STOP. I HAVE INSTALLED NEW ROTORS AND BRAKE PADS ON ALL FOUR SIDES. WHEN TURN ON THE IGNITION, CAR DOESN'T START AT ALL, DOESN'T EVEN MAKE CLICKING SOUND. WHEN TOUCH THE BATTERY COMPARTMENT POSITIVE CHARGE SYSTEM THEN CAR STARTS WITH KEY IGNITION ON. THIS HAPPENS WHEN CAR IS DRIVEN THROUGHOUT THE DAY ASSUMING BATTERY IS FULLY CHARGED. NO LIGHT ATE ON WHEN TRY TO START THE ENGINE.
WIRING TO THE HEAT AND AIR CONDITIONING IS MELTED TOGETHER AND GE FAN DOESN'T WORK ALL THE TIME. DONT HAVE AIR CONDITIONING. AND THE ADAPTERS DONT WORK CANT CHARGE PHONE . ALSO THERE IS A TICKING NOISE COME FROM THE FRONT OF CAR U CAN HEAR IT WHEN IDLING BUT GETS WORSE WHEN U STEP ON THE GAS GOING DOWN THE ROAD.OIL HAS BEEN CHARGED AND IS CHECKED FREQUENTLY. THE NOISE STARTED RIGHT AFTER HAD OIL CHANGE AND TIRES ROTATED.
The contact owns a 2014 Kia Forte. The contact stated that the vehicle was consuming an excessive amount of oil while driving at various speeds. The check engine warning light was illuminated on the instrument panel. The contact had the vehicle taken to an independent mechanic where she discovered that the vehicle had a defective O2 sensor. The contact stated that on another occasion while driving 40 mph, the vehicle began to stall upon the depression of the accelerator pedal. The contact pulled the vehicle into a parking lot and called her husband for assistance. The contact's husband attempted to jump-start the vehicle however, the vehicle failed to restart. The contact then purchased a new battery however, the failure persisted. Due to the failure, the contact had the vehicle towed to a dealer where they diagnosed the vehicle with engine failure. Upon investigation, the contact linked her failure to NHTSA Campaign Number: 20V750000 (Engine) however, her vehicle was not included in the recall. The manufacturer was notified of the failure and provided a case number. The vehicle was not repaired. The failure mileage was unknown.
VEHICLE WAS IN MOTION WHEN THE ELECTRICAL WENT OUT. THE ABS, TRACTION CONTROL, AND STEERING WARNING LIGHTS CAME ON. THE VEHICLE WAS DIFFICULT TO STEER TO THE SIDE OF THE ROAD. CAR HAD 60K MILES. BATTERY IS NOW ON ITS 3RD REPLACEMENT. OTHER PRIOR WARNING SIGNS WERE HEADLIGHTS FLICKERING AND OCCASIONAL CLICKING WHEN STARTING. THESE OTHER PRIOR WARNING SIGNS HAVE OCCURED SINCE 30K MILES.
ENGINE KNOCKING AND THEY REPLACED UNDER WARRANTY. CAR HAD 86,000 MILES. DROVE CAR TO WORK NEXT DAY AND IT CAUGHT ON FIRE WHILE DRIVING HOME ON BUSY HIGHWAY. KIA CORP KNOWS OF A PROBLEM WITH FUEL PUMP AND LINES NEEDING TO BE REPLACED ONCE ENGINE IS REPLACED BUT FAILED TO LET THEIR DEALERSHIPS BE AWARE OF THIS ISSUE. ALSO WHY IS THE FORTE NOT ON RECALL LIST AS MANY KIA FORTES ARE ALSO CATCHING ON FIRE DUE TO ENGINE/ ENGINE REPAIRS.
Data synced from NHTSA on May 4, 2026