There are 5 owner-reported fuel system complaints for the 2000 Nissan Maximain NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
THE CAR STARTED ACCELERATING AND THEN DIED WHILE DRIVING DOWN THE ROAD. HAD TO EXIT OFF THE ROAD FAST AS THE CAR COASTED DOWN TO PREVENT OTHER CARS FROM HITTING THE CAR. IN DANGER OF OTHER CARS RUNNING OVER CAR WHILE OUR CAR MALFUNCTION. TOOK CAR TO SHOP AND WAS TOLD A 2 DOLLAR O-RING ON THE AUTO CONTROL VALVE HAD ALLOWED AIR LEAKAGE AND THIS IN TURNED CAUSED FAILURE OF THE ECM ELECTRON CONTROL MODULE. BOTH AUTO CONTROL VALVE AND ECM NEEDS REPLACING WHERE THE CAR CAN BE SAFELY DRIVEN. THE FACT OF THIS FAILURE DID NOT BRING IN THE ENGINE SERVICE LIGHT TILL AFTER THE EVENT AND FACT IT WILL COST OVER $2000 DOLLARS TO REPAIR A CAR THAT IS NOT WORK MUCH MORE $3000 ARE JUST FACTS. NISSAN NEEDS TO AT LEAST SEND OUT TO THEIR CUSTOMERS THAT OWNS OF THIS MODEL AND MAKE COULD HAVE THIS CONDITION THAN CAN HAPPEN AND EXIST AND CAUSE ERRATIC BEHAVIOR OF THE CAR IF NOT CHECK BY NISSAN. A $2 DOLLAR PART CAUSING A $2000 DOLLAR REPAIR. *TR
I HAVE THE SAME ENGINE IGNITION COIL PROBLEM AS LISTED THROUGHOUT YOUR SITE AND THE INTERNET BY THOUSANDS OF OTHER 2000 NISSAN MAXIMA OWNERS. THE SERVICE ENGINE LIGHT IS ON, THE CAR IS BARELY RUNNING BECAUSE OF THESE FAULTY IGNITION COILS WHICH THE DEALER RECOMMEND I HAVE REPLACED FOR OVER $1000. NISSAN REFUSES TO ADDRESS THIS DEFECT WITH A RECALL. SOMETHING NEEDS TO HAPPEN. FIRST THEY TOLD IT WAS THE SPARK PLUGS WHICH I HAD REPLACED. THEN IT WAS THESE COILS, THE CAR JUST KEEPS GETTING WORSE DAILY. STALLING, BARELY ACCELERATING, CAN'T TAKE IT ON THE HIGHWAY BECAUSE IT BARELY MOVES. ACCELERATOR FAILS OFTEN, SOMETIMES THERE IS NO RESPONSE FROM PUSHING THE GAS PEDAL DOWN. THE FUMES COMING FROM THE CAR INDICATE THAT GAS IS BEING WASTED. ALSO GETTING TERRIBLE GAS MILEAGE. PLEASE HELP. *NM
MY HUSBAND WAS DRIVING THE VEHICLE WHEN HE HEARD A POP AND SAW SMOKE COMING FROM THE CAR. HE PULLED TO THE SIDE OF THE ROAD WHERE THE CAR BECAME ENGULFED IN FLAMES. THE FIREMAN THAT PUT OUT THE FIRE SEEMED TO THINK THE FIRE WAS CAUSED BY A FUEL LINE THAT BURST. *JB
ENGINE STALLS AT IDLE OR WHEN SLOWING DOWN AND THE RPM'S FALL BELOW 600. HAD TO RESTART ENGINE AND KEEP ONE FOOT ON ACCELERATOR AND OTHER ON BRAKE TO KEEP RPM'S ABOVE STALLING POINT. ON WAY TO WORK, I MUST HAVE HAD TO RESTART AT LEAST 25 TIMES AND MULTIPLE MORE TIMES TO GET HOME. HAD TO REPLACE THE ICV OR AAC VALVE AT A COST OF OVER $550 (HAD I GONE TO DEALER); BUT WAS ABLE TO PAY LESS AT AN INDEPENDANT REPAIR SHOP OF $380. THIS PART SHOULD HAVE LASTED LONGER ON MY WELL MAINTAINED VEHICLE.*AK
BROUGHT IN INITIALLY AND ECM WAS RESET. TWO DAYS LATER FAILED AGAIN. ON RETURN FOR SERVICE FUEL INJECTOR #6 WAS REPLACED. TWO DAYS LATER FAILURE OCCURRED AGAIN. ENGINE SERVICE LIGHT IS ON. FEEL THIS IS A SAFETY CONCERN BECAUSE I HAVE NO IDEA IF A MAJOR PROBLEM HAS OCCURRED OR THE SENSOR IS JUST NOT WORKING PROPERLY. *AK
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 25, 2026