There are 6 owner-reported engine complaints for the 2011 GMC Yukonin NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
GMC shuts down while driving. Almost caused 2 accidents. Then it starts back up. Very dangerous!!!
WHILE DRIVING DOWN THE HWY ON APPROXIMATELY 04/08/2020 I HEARD A LOUD POP AND THEN A TICKING SOUND. I PULLED OFF THE SIDE OF THE ROAD TO LOOK AT THE MOTOR TO FIND THAT 4 OF MY EXHAUST MANIFOLD BOLTS WERE BROKEN OFF. BOTH OF THE FRONT AND REAR BOLTS ON BOTH MANIFOLDS WERE MISSING AND THE FRONT PASSENGER SIDE EXHAUST PORT WAS LEAKING. AFTER TAKING IT TO A SHOP TO BE LOOKED AT, THE MECHANIC STATED THAT THIS IS A COMMON PROBLEM WITH GM V8 ENGINES AND HAS BEEN FOR YEARS. THIS ISSUE COULD CAUSE AN ACCIDENT IF SOMEONE GETS OUT OF THEIR VEHICLE ON THE SIDE OF THE ROAD AND THEY OR ANOTHER OPERATOR ISN'T PAYING ATTENTION, SOMEONE COULD GET RUN OVER. I DON'T HAVE ANY PICTURES AS MY SUV IS IN THE SHOP BEING REPAIRED.
TL* THE CONTACT OWNS A 2011 GMC YUKON. WHILE DRIVING 55 MPH, THE ENGINE STALLED AND A LOUD POPPING AND KNOCKING NOISE WAS HEARD. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE CONTACT WAS ABLE TO RESTART THE VEHICLE. THE VEHICLE WAS NOT TAKEN TO A DEALER, BUT WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE LIFTERS IN THE ENGINE WERE DAMAGED AND NEEDED REPLACEMENT. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 177,199.
VALVE LIFTERS NEED REPLACED. RESEARCHED AND THIS IS A COMMON ISSUE SEVERAL PEOPLE ARE HAVING WITH THIS TYPE OF VEHICLE. REPAIR SHOP ALSO SAID A COMMON REPAIR FOR THIS MODEL.
TL* THE CONTACT OWNS A 2011 GMC YUKON. WHILE DRIVING 60 MPH, THE VEHICLE STALLED AND RESTARTED INDEPENDENTLY. THE FAILURE RECURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS TAKEN TO A DEALER, BUT COULD NOT BE DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 70,000.
TL* THE CONTACT OWNS A 2011 GMC YUKON. WHILE DRIVING AT AN UNKNOWN SPEED, THE ENGINE WARNING LIGHT ILLUMINATED AND A LOUD ABNORMAL NOISE WAS HEARD. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE VALVES NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 185,000.
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 25, 2026