There are 35 owner-reported electrical system complaints for the 2010 Chevrolet Camaroin NHTSA's database. These are unverified consumer reports and may not reflect confirmed defects.
The contact owns a 2010 Chevrolet Camaro. The contact stated that the vehicle failed to start after several attempts, with the check engine warning light flashing on the instrument panel. The battery was taken to an independent mechanic where the battery was checked and found to be in good working order. The battery was placed back into the vehicle where the vehicle; however, the vehicle intermittently failed to start after several attempts. Upon investigation, the contact discovered NHTSA Campaign Number: 09V155000 (Electrical System); which the contact linked to the failure. Neither the dealer nor the manufacturer was notified of the failure. The vehicle was not repaired. The failure mileage was approximately 124,000.
The contact owns a 2010 Chevrolet Camaro. The contact stated that while driving at approximately 40 MPH, the driver’s right knee struck the ignition key causing the key to break off inside the ignition switch. The contact was unable to turn the vehicle off. The battery was disconnected. The cause of the failure was not yet determined. The manufacturer was notified of the failure. The local dealer was not yet contacted. The failure mileage was 110,000.
WATER SHORTED THE APP CIRCUITS AND CAUSED THE THROTTLE TO ACTIVATE WITH OUT DRIVER INPUT. WATER IS A POTENTIAL CAUSE FOR SUDDEN UNINTENDED ACCELERATION IN VEHICLES EQUIPPED WITH POTENTIOMETER TYPE APP SENSOR'S THROUGH EXTENSIVE RESEARCH BETWEEN AUGUST 2019 AND SEPTEMBER 2020, I HAVE DETERMINED THAT A WATER INTRUSION PROBLEM INTO THE INSTRUMENT PANEL (IP) TO BODY HARNESS CONNECTOR, WHICH CARRIES THE APP SENSOR SIGNALS TO THE ECM/PCM HAS THE POTENTIAL TO CAUSE SUDDEN UNINTENDED ACCELERATION IN MANY OF THE 2005-2018 GM PRODUCT LINE. WATER CAN ENTER THE CONNECTOR THROUGH BODY LEAKS AND MAY CAUSE AN INCREASE IN VOLTAGE ON APP 1 AND APP 2. ON SOME VEHICLES THIS CAN ALSO CAUSE A MALFUNCTION IN THE BPP/BRAKE SWITCH STATUS CIRCUIT. AS A RESULT THIS MALFUNCTION CAN MISTAKENLY APPEAR AS A PEDAL MISAPPLICATION IN THE EDR REPORT FROM THE SDM. THIS FINDING APPLIES TO MANY OTHER VEHICLE USING A POTENTIOMETER TYPE APP SENSOR BUT THE RESEARCH WAS DONE SPECIFICALLY ON GM VEHICLES. I HAVE ALSO DETERMINED WATER INTRUSION INTO THE CONNECTOR 109 ON THE FULL SIZE TRUCK LINE HAS THE POSSIBILITY TO CAUSE FALSE ACTIVATION OF THE APP CIRCUIT. USING WATER I HAVE CONFIRMED THAT WATER CAN CAUSE THE VOLTAGE INCREASE ON APP CIRCUIT 1 AND APP CIRCUIT 2 AND NOT ENTER REDUCED POWER MODE, IT ALL COMES DOWN TO SURFACE AREA EXPOSED AND SODIUM CONTENT IN THE WATER AS TO THE FINAL RESULTS. AS THESE VEHICLES BECOME OLDER THE LIKELY HOOD OF THESE EVENTS OCCURRING INCREASES. VEHICLES NEAR SALT WATER OR WHERE SALT IS USED ON THE ROADS ARE MORE LIKELY TO FAIL WITH HIGHER APP %. BECAUSE OF THE KNOWN WATER LEAK INTO THE CONNECTOR'S CONTAINING APP WIRES AND VERIFICATION THAT WATER CAN CAUSE FALSE ACTIVATION OF THE APP CIRCUITS. IT IS MY CONCLUSION IN RARE EVENTS THIS WATER COULD CAUSE FALSE ACTIVATION OF BOTH APP SIGNAL IN MANY OF THE 2005-2018 GM VEHICLES. THIS VEHICLE WAS USED FOR CONFIRMATION.
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT STATED THAT THE KEY BECAME STUCK IN THE IGNITION. THE CONTACT HAD TO TURN THE STEERING WHEEL AND APPLY THE EMERGENCY BRAKE TO RELEASE THE KEY. THE CONTACT STATED THAT SHIFTING THE GEARS WHILE DEPRESSING THE BRAKE PEDAL HELPED SOMETIMES DURING THE FAILURE. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE CONTACT CALLED SHOTTENKIRK CHEVROLET (5031 AVENUE O, FORT MADISON, IA 52627, (319) 248-8866), BUT NO ASSISTANCE WAS PROVIDED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND DID NOT ASSIST. THE FAILURE MILEAGE WAS 52,000.
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. WHILE DRIVING APPROXIMATELY 35 MPH, THE ODOR OF BURNING PLASTIC WAS PRESENT. TWO DAYS LATER, THE WARNING INDICATOR FOR THE EXTERIOR LIGHTING ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER (ROGER DEAN CHEVROLET, 101 SW PINE ISLAND ROAD, CAPE CORAL, FL 33991) FOR DIAGNOSTIC TESTING AND REPAIRS. THE DIAGNOSIS WAS NOT PROVIDED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 74,977.
I was in an accident with a friend in [XXX] We weren't doing over 30 to 35 miles per hour when we hit a deer. All I could remember was yelling because my wrist was broken and I had bone coming out from the air bags that deployed on my side of the car. The wind shield was cracked because of this as well. My friend had to jump out of the car to disconnect the battery because the car would not shut off or stop moving. The brake and parking brake was used but couldn't get it to stop. My friend had to crawl out the side window by them to let me out of the car because neither door opened to let us out. My friend was hurt as well but not as bad as my wrist. The er doctor told me since my wrist never healed or would ever heal correctly. That iwould have to go see a hand specialist to do surgery and put pins in but wasn't a guarantee fix. Till this day I have trouble working if it requires me to pick up heavy things with that hand because I just feel the pain and how it feels like it wants to come apart. This happened in bandera Texas on [XXX]. I did make a police report and even claimed it on my insurance. I was told the car was totaled due to cost of the air bags being deployed. I have not reported to anyone because people don't think it is a safety issue. So I'm still have debit from this incident that I don't want anyone to have to go through what I have since that day. I was seen at beorne Methodist er in beorne texas. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)
IN FIRST THREE YEARS, THE ELECTRONIC IGNITION MODULE WAS REPLACED THREE TIMES. ON THE THIRD TIME, IT WAS FOUND THAT THE IGNITION WIRING HARNESS WAS NOT FOR A CAMARO. IT WAS INCORRECTLY INSTALLED AT THE FACTORY. SECONDLY, JUST THREE WEEKS AGO, FOUR OF MY CAR'S SIX FUEL INJECTORS WENT BAD. MY CAR ONLY HAD 74,000 MILES ON IT. ALL SIX INJECTORS WERE REPLACED AT MY COST OF $2812.00! OUTRAGEOUS! BOTH TIMES, MY CAR WAS BEING DRIVEN ON A CITY STREET.
MANUAL DRIVER'S SEATBACK WENT FORWARD ON ITS OWN & STUCK IN FORWARD POSITION AND TRUNK POPPED ON ITS OWN WHILE STATIONARY. 2010 CAMARO 2LT HADN'T BEEN DRIVEN OVER CHRISTMAS BREAK. WHILE OUT STROLLING, MY HUSBAND STOPS TO CRANK THE CAR SINCE IT HAD BEEN SITTING FOR A COUPLE OF WEEKS. HE GOT IN, CRANKED IT. NO TROUBLE. A WEEK LATER I WENT TO DRIVE IT TO WORK, USED REMOTE KEY TO UNLOCK DOORS AND NOTICED THE SEATBACK WAS STUCK CLOSE TO THE STEERING WHEEL. I TRIED LATCH ON SEAT'S BACK AND SIDE LEVER, BUT COULDN'T GET THE SEATBACK TO MOVE. I CALLED TO TELL MY HUSBAND I WAS TAKING OUR OTHER VEHICLE TO WORK AND ASKED IF HE'D RAISED THE SEATBACK THE DAY HE CRANKED THE CAR FOR GOOD MEASURE. HE DIDN'T RECALL DOING SO. LATER THAT EVENING, WE WENT TO LOOK AT THE CAR TOGETHER, USED THE REMOTE TO UNLOCK THE DOORS. HE TRIED MOVING THE SEATBACK AND COULDN'T. HE NOTICED THE TRUNK WAS POPPED AND ASKED IF I'D POPPED IT. I DIDN'T THINK SO, BUT MAYBE I HIT THE WRONG BUTTON WHEN UNLOCKING THE DOORS. HE SLAMMED THE TRUNK SHUT. WE THOUGHT PERHAPS HE FORGOT TO LOCK THE CAR AND SOMEONE HAD RUMMAGED THROUGH OUR CAR AND JAMMED THE SEAT. A BRIEF ONLINE SEARCH REVEALED OTHER CAMARO OWNERS W/ SAME ISSUE. THE SEATBACK HAD GONE FORWARD ON ITS OWN. I THOUGHT, IF SEATBACKS ARE MOVING FORWARD ON THEIR OWN WHAT HAPPENS IF SOMEONE'S DRIVING. UNSAFE! I VISITED NHTSA ONLINE AND SAW PICTURES ARE HELPFUL. I WENT HOME TO TAKE A PIC. THIS TIME THE REMOTE DIDN'T UNLOCK THE DOORS, SO I USED THE KEY. AFTER PHOTOS, I NOTICED THAT THE TRUNK WAS POPPED AGAIN. NO WAY I 'HIT THE WRONG BUTTON,' THE REMOTE WASN'T WORKING. I CHECKED TRUNK AND NOTED THE INSIDE LIGHTS WEREN'T ON. THE CAR'S BATTERY HAD DRAINED FROM THE TRUNK BEING OPEN FOR EXTENDED PERIODS OF TIME ON TWO SEPARATE OCCASIONS. SEATBACK MOVING FORWARD ON ITS OWN AND TRUNK POPPING ON ITS OWN'NOT A COINCIDENCE. BOTH ARE SERIOUS SAFETY CONCERNS. *TR
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT STATED THAT WHILE DRIVING, THE INTERIOR LIGHTS IN THE VEHICLE FLICKERED. IN ADDITION, THE FRONT HEADLAMPS ALSO FLICKERED. THE CONTACT ALSO STATED THAT THE CHECK ENGINE WARNING LIGHT REMAINED ILLUMINATED WHILE DRIVING WHICH CAUSED THE VEHICLE TO DRIVE ROUGH. THE VEHICLE WAS TAKEN TO SIMPSON CHEVROLET LOCATED AT 10150 TRASK AVE, GARDEN GROVE, CA 92843, AND THE ECU WAS RESET HOWEVER, THE FAILURE PERSISTED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 37,000.*DT*DT*JB
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT STATED THAT WHILE PARKED, THE AIR BAG WARNING LIGHT ILLUMINATED. THE CONTACT STATED THAT THE FAILURE OCCURRED WHEN DRIVING OR PARKED ALONG WITH A CHIME. THE VEHICLE WAS TAKEN TO A DEALER WHERE IT WAS DIAGNOSED THAT THE AIR BAG SENSOR AND MODULE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 42,600.
The contact owns a 2010 Chevrolet Camaro. The contact received a notification for NHTSA Campaign Number: 14V364000 (Electrical System). The dealer was notified about the recall and the vehicle was dropped off for the recall repair. The next day, the contact was informed that the parts were on backorder and to pick up the vehicle. The manufacturer had been notified of the recall. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall. repair. The contact had not experienced a failure. Parts distribution disconnect.
TL*THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT STATED THAT THE VEHICLE STALLED SEVERAL TIMES WITHOUT ANY WARNING. THE CONTACT MENTIONED THAT THE INSTRUMENT PANEL FLICKERED FOR ALL OF THE GAUGES AND THE SENSORS INDICATING THAT THERE WAS SOME SORT OF ELECTRICAL SHORT. THE CONTACT STATED THAT AFTER INSPECTING THE VEHICLE, IT WAS NOTICED THAT THERE WAS A WATER LEAK IN THE TRUNK. IN ADDITION, THE CONTACT STATED THAT THE KEY BECAME LODGED IN THE IGNITION SWITCH AND THE BRAKE PEDAL FAILED TO DEPRESS. THE VEHICLE WAS TOWED TO AN AUTHORIZED DEALER, WHO DIAGNOSED THAT THERE WAS CORROSION AROUND THE TERMINALS AND THE POWER CIRCUIT. THE TECHNICIAN WAS UNABLE TO IDENTIFY THE SOURCE OF THE LEAK AND DIAGNOSED THAT THE ELECTRICAL WIRING HARNESS NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS NOT AVAILABLE.
DUE TO A STRUCTURAL DEFECT OF THE CAR , WATER ACCUMULATED AND THE ELECTRICAL SYSTEM FAILED COMPLETELY. THE DEALERSHIP IDENTIFIED THAT THERE WAS A STRUCTURAL DEFECT RELATED TO THE SUNROOF . THE CAR COMPLETELY LOST ALL POWER SINCE THE ELECTRICAL SYSTEM FAILED . THEREFORE THERE WAS NO POWER STEERING , AND I WAS UNABLE TO EXIT THE CAR SINCE ALL POWER FAILED . THIS WAS AN IMMEDIATE LIFE THREATENING DANGER . THE DEALERSHIP " REPAIRED " THE PROBLEM AFTER AN EXTENSIVE ASSESSMENT WHICH INCLUDED CORRESPONDENCE WITH GENERAL MOTORS . THE COST OF THE REPAIR WAS $1200 . MY CONCERN IS THAT THIS MAY BE A LIFE THREATENING SAFETY HAZARD IN OTHER VEHICLES OF THE SAME MAKE AND MODEL . I WOULD ALSO LIKE TO BE REIMBURSED THE FULL AMOUNT OF THIS REPAIR SINCE THIS WAS A MANUFACTURER DEFECT . THE OUTCOME OF THIS COULD HAVE BEEN CATASTROPHIC . PLEASE ADVISE ME ON HOW I WOULD IMPLEMENT THE PROCESS OF REIMBURSEMENT . *TR
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 14V346000 (ELECTRICAL SYSTEM). THE CONTACT STATED THAT THE REPAIR WAS PERFORMED; HOWEVER, THE REMOTE WAS DAMAGED DURING THE REPAIR. THE CONTACT STATED THAT HE PAID FOR A NEW REMOTE, BUT THE NEW REMOTE WAS A PRE-RECALL REMOTE. THE REMOTE WAS NON-COMPLIANT WITH THE RECALL. THE FAILURE MILEAGE WAS UNKNOWN. UPDATED 09/10/15*LJ
TL*THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT STATED THAT THE TRUNK WIRE SEPARATED AND FAILED TO OPERATE. THE VEHICLE WAS TAKEN TO A DEALER, WHO DIAGNOSED THAT AFTER NUMEROUS CYCLES THE WIRES SEPARATED AND NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 48,000.
2010 CHEVROLET CAMARO. CONSUMER WRITES IN REGARDS TO GM IGNITION RECALL* THE CONSUMER STATED THE REPAIR WAS NOT ACTUALLY A FIX AT ALL. PORTIONS OF THE KEY WERE REMOVED AND A SEPARATE KEY WAS ATTACHED BY TWO SMALL KEYS RINGS. THE IGNITION WAS NOT REPAIRED IN ANY WAY. *JB
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT STATED THAT THE ELECTRICAL DRIVER SEAT ADJUSTER FAILED TO MOVE THE SEAT. THE VEHICLE WAS TAKEN TO THE DEALER. THE TECHNICIAN DIAGNOSED THAT THE SEAT BOTTOM AND DRIVER MOTOR SWITCH NEEDED TO BE REPLACED. THE REPAIRS WERE MADE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 42,936. UPDATED 04/10/15*LJ
TRUNK LATCH JUST STOPPED OPENING TRUNK. IT STILL MAKE THE SOUND THAT IT ALWAYS MADE BUT IT DOESN'T RELEASE THE LID. THE ONLY WAY TO OPEN THE TRUNK IS TO PULL THE EMERGENCY TRUNK RELEASE INSIDE THE TRUNK AS THERE IS NO MANUAL KEY OPERATED RELEASE OF THE TRUNK FROM THE OUTSIDE OF THE TRUNK. MANY OTHERS HAVE VOICED THIS EXACT COMPLAINT POSTED ONLINE ON AUTOMOBILE FORUMS. ALSO REPLACING THE BULBS IN THE HEADLIGHTS SEEMS TO PRODUCE VERY POOR LIGHT FOR NIGHT TIME DRIVING. THE REPLACEMENT BULBS WERE 4300K HID BULBS 35W JUST LIKE THE ORIGINAL MANUFACTURERS EQUIPMENT, PURCHASED FROM A VERY RESPECTABLE PARTS SUPPLY COMPANY. *TR
LICENSE PLATE LIGHTS OVERHEATED AND MELTED THROUGH THEIR RESPECTIVE ASSEMBLIES. THE HEAT ALSO CAUSED THE REAR PLASTIC BUMPER TO MELT IN A SMALL AREA AT ONE ASSEMBLY. *TR
TL* THE CONTACT OWNS A 2010 CHEVROLET CAMARO. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 14V346000 (ELECTRICAL SYSTEM); HOWEVER, THE PART NEEDED TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED THE FAILURE. UPDATED 7/9/15*CN UPDATED 10/11/2017*CN
Showing 1–20 of 35 complaints
Complaints are unverified consumer reports submitted to NHTSA. A high complaint count may reflect vehicle popularity, not defect severity. Data sourced from NHTSA public records.
Data synced from NHTSA on Apr 25, 2026