NHTSA Owner Complaint Log
This page lists owner-reported complaints filed with NHTSA for the 2008 Ford F-350. Complaints are unverified consumer reports submitted to NHTSA and do not by themselves prove a defect or defect rate.
Data synced from NHTSA on May 4, 2026
I have had multiple incidents of my truck shutting off completely while driving. The latest incident resulted in a "catastrophic engine failure". In the latest incident occurring in April 2025, I was driving on [XXX] . [XXX] is a two-lane highway with no divider, navigating through mountainous terrain. I was driving up a hilly area when my truck shut off, and I lost all power steering. There is no shoulder on this part of the freeway, with an approximate 40-foot embankment. I was able to navigate the vehicle to the side of the road and position it just before the beginning of a guard rail beginning allowing me some grace. Due to no shoulder space, I was effectively parked on the white containment line of the road. I had my [XXX] daughter and wife in the car. I had to wait for a break in traffic to be able to open the driver's door due to the proximity to the active highway. I was safely get the truck towed to the nearest FORD dealership, where it was determined the engine was in "catastrophic failure" due to oil engine overfill. I informed FORD that my last oil change was with the FORD dealership and within the recommended time frame. I was informed by a technician that there is an ongoing issue with this engine make (6.4-liter, diesel). The technician stated that FORD is aware of the issue. The technician stated that fuel gets mixed with the oil and causes an "engine oil overfill". None of these issues stems from negligence but rather an unakknowledged issue by FORD. There was a check engine light that appeared at the time of failure. The check engine light had come on, at which point I contacted a mechanic to schedule an appointment. When I arrived for my appointment, the check engine light had disappeared, and I was told that no codes would alert if the actual check engine light was not on during the inspection. That same scenario occurred on approximately 3 occasions. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)
Vehicle died while driving on the freeway. Towed to the local Ford who did a diagnostic and test they found that the engine is completely done with as there was an engine oil overfill, and it filled the CAC system and melted cylinder eight piston. they’re saying that they will need to replace the entire engine and HP fuel pump in order to repair and I see many others have experienced this same problem.
Items inside bed caught on fire due to exhaust cleaning system getting so hot to burn off pollution in DPF pipe. Dangerous truck to drive contacted ford. No one contacted me. Other ford diesels caught on fire due to this. I’m retired military and don’t have money to buy 50k trucks. Only 80k on truck.
Death wobble. First experience was September 2019
The contact owns a 2008 Ford F-350. The contact stated that on several occasions while the accelerator pedal was depressed, the contact noticed a burning odor throughout the vehicle. The contact stated that the rear driver’s and passenger’s side wheels inadvertently locked without warning then released. No warning lights were illuminated. The vehicle was taken to the dealer where the brake pedal and plunger rod was replaced with a longer plunger rod; however, the failure recurred. The contact stated that while driving at an undisclosed speed, he depressed the brake pedal however, the vehicle failed to stop. The contact stated that he had to applied pressure to the brake pedal that was depressed down to the floorboard. As a result, the vehicle glided to a stop. No warning lights were illuminated. The vehicle was taken back to the dealer where it was diagnosed that brake pedal and the brake master cylinder needed to be replaced. The vehicle was repaired; however, the failure recurred after the vehicle was retrieved from the dealer. The contact stated that while the accelerator pedal was depressed, the front driver’s side wheel locked without warning and then released. The contact stated that he steered the vehicle off the roadway and was informed by another motorist that there was smoke underneath the vehicle. The contact stated that he was assist by Law Enforcement and advised to call the NHTSA Hotline. The vehicle was then taken back to the dealer where it was diagnosed that the brake caliper, front brake lock, brake pads, master cylinder and other undisclosed brake parts needed to be replaced. The vehicle was repaired; however, the failure recurred. The contact was advised by the technician to take the vehicle to Bob’s 151 transmission Center where it was diagnosed that the ABS had failed and needed to be replaced. The vehicle was not repaired. The manufacturer was notified of the failure and the contact was informed that the vehicle was too old, and no further assistance was provided. The contact stated that the call was disconnected. The failure mileage was approximately 70,000
Steering went out , wouldn’t return to center
Power steering pump replaced with new unit. Major steering issues. Will not turn at some points. Almost caused 3 accidents on 10/22/2021. Have had front end and power steering pump replaced.
Death wobble and learned about class action after I had front end repaired with complete overhaul ball joints etc in January 2018 ($2100 plus dollars) by my mechanic. May 16, 2021 experienced 3 incidents of death wobble in Oklahoma City enroute toTulsa, Oklahoma. See my mechanic on June 1, 2021.
ON INTERSTATE PASSING IN LEFT LANE HIT A ROUGH PATCH TRUCKS STARTS SHAKING SO BAD I THOUGHT IT WAS GOING TO FLIP. COULD NOT GET TO SHOULDER SO HAD TO GO IN THE MEDIAM IT WAS NOT A FLAT SPOT IT WAS A HILL SO I WENT STRAIGHT AND NOT AT AN ANGLE IF I HAD I WOULD OF FLIPPED. THIS IS NOT THE FIRST TIME. IFRIST TIME I HAD APPROX $3000.00 OF FRONT IN WORK DONE TRYING TO FIX THE PROBLEM, BUT IT DID NOT.
DEATH WOBBLE-ERRATIC DRIVING WHEN THIS HAPPENED IT WAS IN MOTION ON A HIGHWAY.
WE WERE HAULING A LOAD OF LOGS ABOUT AN HOUR AWAY EVERYTHING WAS FINE WHEN ALL OF THE SUDDEN THE TRUCK DOWN SHIFTED AND WHITE SMOKE STARTED POURING OUT FROM UNDER THE PASSENGER SIDE OF THE HOOD FOLLOWED BY FLAMES. WE HAD TO TRY TO GET OFF THE ROAD WHERE WE WERE THERE WAS NO WHERE TO PULL OFF AND FINALLY COULD SWING INTO A STATE GAMESLAND AND SOMEONE CALLED THE FIRE DEPT. I AM NOW OUT OF A TRUCK I JUST PURCHASED 2 MONTHS AGO AND MY VIN NUMBER ISN'T EVEN SHOWING UP
TL* THE CONTACT OWNS A 2019 FORD F-350 SD, EQUIPPED WITH MICHELIN TIRES, TIRE LINE: LTX MS/2, TIRE SIZE: 245/75/R17, DOT NUMBER: B74345 (PARTIAL). THE CONTACT STATED WHILE DRIVING 75 MPH, THE FRONT DRIVER'S SIDE TIRE WENT FLAT AND THE STEERING CEASED. THE CONTACT DEPRESSED THE BRAKE PEDAL AND PULLED OVER TO THE SIDE OF THE ROADWAY. THE TIRE WAS REPLACED WITH THE SPARE TIRE. THE CONTACT STATED THAT IT WAS THE SECOND TIME THE FAILURE OCCURRED. THE FIRST TIME, THE FRONT PASSENGER SIDE TIRE WENT FLAT WHILE THE CONTACT WAS DRIVING AT AN UNDISCLOSED SPEED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND INFORMED THAT THERE WAS NO RECALL AND THAT THE TIRE WAS OVER THE WARRANTY COVERAGE PERIOD. THE FAILURE MILEAGE WAS 54,000. THE VIN WAS UNAVAILABLE.
DRIVING THRU TOWN 25MPH OR LESS TURNING ONE CORNER FINE THEN ANOTHER CORNER THE OPPOSITE DIRECTION AND ONLY STEERING WHEEL TURNED.MY TRUCK WENT STRAIGHT INTO THE ROCK WALL DAMAGED HOOD FENDER,BUMPER,HEADLIGHT BEZEL AND LIGHTS DRIVER WHEEL, AND WHEN DIAGNOSED THE ORIGINAL PROBLEM IT WAS THE STEERING GEARBOX FAILURE
DEATH WOBBLE OCCURS AT HIGHWAY SPEEDS IF BUMPS OCCUR CONSECUTIVELY CLOSE TOGETHER,THE ONLY WAY TO STOP WOBBLE IF YOU ABRUPTLY STOP,IT'S WORSE IF YOUR ON A TRANSITION RAMP TO ON COMING TRAFFIC.
TL* THE CONTACT OWNS A 2008 FORD F-350. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS, THE POWER STEERING AND BRAKING SYSTEM WOULD SUDDENLY MALFUNCTION CAUSING THE DRIVER TO NEARLY LOOSE CONTROL OF THE VEHICLE. DURING THE FAILURES, THE STEERING WHEEL WOULD NOT TURN IN EITHER DIRECTION AND THE BRAKE PEDAL WAS DIFFICULT TO DEPRESS. THE CAUSE OF THE FAILURES WERE NOT DETERMINED. THE LOCAL DEALER TAYLOR MOTOR COMPANY LOCATED AT 524 RUSS AVE, WAYNESVILLE, NC 28786 WAS NOTIFIED OF THE FAILURE. THE MANUFACTURER WAS NOT CONTACTED. THE FAILURE MILEAGE WAS 211,000.
I HAVE A 2008 FORD F-350 THAT I EXPERIENCED A VIOLENT, SHUDDERING, VIBRATION AT APPROXIMATELY 75 M.P.H. ON INTERSTATE-75 YESTERDAY, 09/19/2020, THAT ALMOST CAUSED ME TO CRASH. I LOOKED ONLINE AND THERE ARE MANY, MANY PEOPLE WHO HAVE AND ARE EXPERIENCING THE SAME, DANGEROUS PROBLEM. I FIRMLY BELIEVE THAT THERE SHOULD BE A RECALL OF THE AFFECTED F-250 AND F-350 VEHICLES AND FORD SHOULD REPAIRS THESE VEHICLES BEFORE ANYONE IS INJURED OR KILLED, IF THERE HASN'T BEEN SUCH A TRAJEDY OR TRAGEDIES ALREADY.
TL* THE CONTACT OWNS A 2008 FORD F-350. THE CONTACT STATED THAT WHILE DRIVING 35 MPH, THE VEHICLE EXPERIENCED THE DEATH WOBBLE. THE CONTACT STATED THAT THE STEERING WHEEL SHOOK VIOLENTLY TO THE LEFT AND TO THE RIGHT. THE CONTACT SLOWED DOWN TO REGAIN CONTROL OF THE VEHICLE. THE CONTACT STATED THAT THE FAILURE RECURRED WHILE DRIVING OVER A BUMPY ROAD SURFACE. BEACH FORD (2717 VIRGINIA BEACH BLVD, VIRGINIA BEACH, VA 23452; 757-486-2717) WAS CONTACTED AND THE CONTACT WAS INFORMED THAT THE VEHICLE WAS NOT SUBJECTED TO A RECALL. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 207,000.
CRUSE CONTROL SWITCH ON THE BRAKE MASTER CYLINDER DISINTEGRATED, CAUSING IMMEDIATE LOSS OF BRAKE FLUID AND BRAKING. SWITCH BODY APPEARED RUSTY, WHILE THE SWITCH NEXT TO IT ON THE MASTER CYLINDER DID NOT. VEHICLE IN MOTION, DESCENDING DRIVEWAY WHEN BRAKE PEDAL WENT TO THE FLOOR AND ALL BRAKING ACTION WAS LOST. VEHICLE STOPPED VIA EMERGENCY BRAKE.
DRIVING DOWN THE ROAD AT 65 MPH, ON OPEN HIGHWAY GOING STRAIGHT, AND ON CRUISE CONTROL, MY SUN ROOF EXPLODED. IF I HAD NOT HAD THE SUN SHADE PULLED CLOSED, WE WOULD HAVE BEEN SHOWERED IN GLASS! I HAD A TRUCK CAMPER ON THE TRUCK AT THE TIME, HOWEVER, I'VE DRIVEN TENS OF THOUSANDS OF MILES WITH THIS CAMPER, SO IT SHOULDN'T BE THAT - AND THE GLASS OUGHT TO BE STRONG ENOUGH FOR THIS USAGE ANYWAY. THIS SHOULD NOT HAVE HAPPENED, AND THE TYPE OF GLASS THAT IS USED SHOULD NOT ALLOW GLASS TO SHATTER INTO FLYING PIECES LIKE THAT! THIS IS COSTING ME A BUNDLE OF MONEY TO REPAIR, BUT MORE IMPORTANTLY, HAD THE SUN SHADE NOT BEEN CLOSED, I COULD HAVE HAD AN ACCIDENT WITH 6+ TONS OF TRUCK AND CAMPER.
I WAS IN MY DRIVEWAY AND STEPPED ON THE BRAKE PEDAL TO PUT THE TRUCK IN REVERSE AND I HEARD A LOUD 'POP' WHICH FELT LIKE THE BRAKE PEDAL BROKE AND THEN IT SANK TO THE FLOOR, I POPPED THE HOOD AND SAW BRAKE FLUID DRIPPING FROM THE BOTTOM OF THE BRAKE MASTER CYLINDER. THIS PART---"SWITCH ASSY - FORD PART-SW6349 (9F924)" HAD BLOWN OUT THE PLASTIC CONNECTOR WHILE THE METAL CASING WAS STILL ATTACHED TO THE BOTTOM OF THE MASTER CYLINDER. THIS WILL LEAVE YOU WITH NO BRAKES. IF IT HAPPENED ON THE ROAD IN TRAFFIC IT COULD BE DEADLY.
HAD THE TRUCK OVER HEAT MULTIPLE TIMES. HAD TO CHANGE THE COOLANT AND ALSO THE RADIATOR ON LONG WITH THE OIL COOLANT CONTAINER. HAS A TICKING SOUND AND HAS NOT YET GONE AWAY. HAVE TAKEN IT TO FORD DEALER AND THEY CAN'T FIGURE IT OUT. WOULD LIKE TO KNOW WHAT TO DO SINCE I HAVE SPENT A LOT OF MONEY AND THE PROBLEM HASN'T BEEN FIXED AND THE ONLY THING THE FORD DEALER TELLS ME IS TO TRADE IT IN FOR A NEW ONE. HELP1
HAD JUST BACK THE VEHICLE IN CUT IT OFF, HALF AN HOUR LATER IT WAS IN FLAMES, BURNT EVERYTHING IN THE MOTOR AND FRONT OF TRUCK UP. *DT*JB *DT*JB *DT*JB *TR
JUST GOT ON THE ON RAMP TO GET ON THE FREEWAY WHEN LOST TOTAL CONTROL OF THE TRUCKS POWERSTEERING. I WAS GOING MAYBE 35-45MPH BUT HAD TO SLOW DOWN. TOOK TO THE FORD DEALER THE REPLACED THE GEARBOX WITH A REMANUFACTURED GEARBOX AND DID THE SAME THING ON MY SECOND TRIP. NOT SURE WHAT TO DO AS THIS IS A BIG SAFETY CONCERN
THE STEERING IS HARD TO TURN I HAVE TO WRESTLE WITH IT VERY OFTEN..
THE 2008, AS WELL AS OTHER YEARS OF THE FORD F-350 ARE KNOWN TO HAVE A PROBLEM WITH A FRONT-END SHIMMY OR "DEATH WOBBLE". I HAVE HAD SEVERAL THOUSAND DOLLARS OF WORK DONE TO MY F-350 IN ORDER TO RESOLVE THE DEATH WOBBLE PROBLEM. THE REPAIRS WORK FOR A TIME AND THEN, WITHOUT WARNING, THE DEATH WOBBLE RETURNS. THE FACT THAT THIS CAN OCCUR WITHOUT WARNING, AT HIGH SPEEDS, BY DRIVING OVER A VERY SMALL BUMP IN THE ROAD, MAKES THIS AN EXTRAORDINARILY DANGEROUS PROBLEM. I DON'T THINK I CAN ADEQUATELY DESCRIBE THE EXTREME NATURE OF THE DEATH WOBBLE. THE FRONT-END OF THE TRUCK IS BOUNCING LEFT AND RIGHT, THE ENTIRE VEHICLE IS TWISTING AND ROLLING, THE STEERING WHEEL IS BARELY CONTROLLABLE, ANYTHING LOOSE IN THE PASSENGER COMPARTMENT GOES FLYING AND KEEPING THE VEHICLE IN ITS LANE IS NOT ALWAYS POSSIBLE. REDUCING SPEED AS QUICKLY AS POSSIBLE IS THE ONLY RECOURSE AND THIS POSES A DANGER PARTICULARLY WHEN ON A HEAVILY TRAFFICKED HIGHWAY. THIS PROBLEM HAS BEEN KNOWN ABOUT FOR A LONG TIME AND FORD WILL NOT TAKE ANY RESPONSIBILITY. EVEN AFTER SPENDING THOUSANDS OF DOLLARS ON COMPLETE FRONT-END REBUILDS, AND IMPECCABLE MAINTENANCE, THE PROBLEM WILL SUDDENLY REOCCUR. THE DESIGN OF THIS FRONT-END IS FAULTY AND VEHICLE OWNERS SHOULD NOT CONTINUE TO BE RESPONSIBLE FOR THE COSTS OF MAINTAINING THIS FAULTY DESIGN AND BEING EXPOSED TO GREAT RISK.
WHILE DRIVING OVER 40 MPH IF A BUMP OR POTHOLE IS HIT THE TRUCK BOUNCES OR SHAKES VIOLENTLY AT THE FRONT. THE TRUCK HAD PREVIOUSLY DONE IT ONE OTHER TIME. THIS TIME THE TRUCK WAS TRAVEING ABOUT 55 MPH ON A 2 LANE HIGHWAY WHEN I HIT A DIP IN THE ROAD AND THE TRUCK STARTED VIOLENTLY BOUNCING AND WENT ACROSS THE OPPOSITE DIRECTION SIDE OF THE HIGHWAY. LUCKILY NO OTHER CAR WAS COMING BUT DAMAGE WAS DONE TO THE FRONT OF THE TRUCK WHEN IT WENT TO THE OPPOSITE SIDE OF THE ROADWAY. I HAVE SINCE PARKED THE VEHICLE UNTIL IT CAN BE FOUND WHAT CAUSED THE PROBLEM. I WILL HAVE TO CONTACT THE INSURANCE CO ABOUT THE FRONT END REPAIR BUT NOT UNTIL IT IS SAFE TO DRIVE.
THE TRUCK SHAKES A LOT WHEN GOING OVER BUMPS ON THE ROAD , AROUND 60 MPH .
AFTER HITTING A BUMP IN THE ROAD, THE TRUCK WILL SHAKE VIOLENTLY AND ATTEMPT TO GET OUT OF CONTROL. THE ONLY WAY TO CORRECT THIS IS BRING THE VEHICLE SPEED DOWN TO UNDER 20 MPH. THIS PROBLEM BEGAN OCCURRING SPORADICALLY ABOUT ONE YEAR AGO AND HAS GOTTEN CONSISTENTLY WORSE. IT IS SO SEVER THAT I HAVE DECIDED TO PARK THE VEHICLE OUT OF A CONCERN FOR SAFETY. I HAD THE VEHICLE INSPECTED AT THE LOCAL FORD DEALERSHIP APPROXIMATELY 3-4 MONTHS AGO AND THEY SAID EVERYTHING WAS FINE. TODAY, I RECEIVED IN THE MAIL A NOTICE MARKED "SPECIAL FIELD ACTION 09L02" THAT SAYS THE PROBLEM IS DUE TO TIRE INFLATION. I HAVE THE PROPER SIZE TIRES AND I KEEP THEM PROPERLY INFLATED. AFTER RESEARCHING THIS, I HAVE NOTICED THAT THIS PROBLEM DATES BACK TO 2005 AND FORD HAS SENT THIS SAME NOTICE OUT MANY TIMES. IT IS NOT A TIRE PROBLEM. I BELIEVE IT IS A KNOWN SUSPENSION PROBLEM AND IT IS DANGEROUS. THIS NEEDS TO BE A MANDATORY RECALL AND IT NEEDS TO BE PAID FOR BY FORD. I CALLED THEIR SERVICE LINE TODAY AND WAS TOLD MY VEHICLE WASN'T PART OF ANY NOTICE OR RECALL. THE PAPER I GOT TODAY SAYS "THIS NOTICE APPLIES TO YOUR VEHICLE" AND GOES ON TO GIVE MY VIN #. IT IS A BIG PROBLEM AND NOW IT HAS A BIG COVER-UP TO GO WITH IT.
THE POWER STEERING PUMP STARTED MAKING A NOISE. THE RESERVOIR WAS EMPTY. I FILLED IT UP ABOUT 100 MILES LATER. STEERING WHEEL STARTED HAVING A LOT OF PLAY IN IT BEFORE TURNING THE WHEELS. ON THE WAY TO THE DEALER TO HAVE IT CHECKED OUT, LOST ALL POWER STEERING. I HAD TO CALL A ROLLBACK TO CARRY IT TO DEALER. THIS IS A 2008 F350 WITH APPROXIMATELY 38,000 MILES ON IT. DEALER INFORMED ME IT WILL COST ME $1500 TO REPLACE THE GEAR BOX PLUS $75 TOWING. I FEEL LIKE THIS IS A FACTORY DEFECT AND FORD MOTOR CO. SHOULD PAY FOR ALL REPAIRS. I NEED ADVICE AND HELP TO RESOLVE THIS COMPLAINT.
TL* THE CONTACT OWNED A 2008 FORD F-350. WHILE DRIVING 25 MPH, THE STEERING ABILITY FAILED ON THE VEHICLE. THE CONTACT LOST CONTROL OF THE VEHICLE AND CRASHED INTO THE WALL OF A BRIDGE. THE CRASH OCCURRED ON JANUARY 11, 2018. A POLICE REPORT WAS FILED. THE CONTACT WAS INJURED AND REQUIRED MEDICAL ATTENTION. THERE WERE NO WARNINGS INDICATORS ILLUMINATED BEFORE THE FAILURE. THE VEHICLE WAS NOT TAKEN TO A DEALER OR INDEPENDENT MECHANIC. THE VEHICLE WAS DESTROYED AND TOWED. THE CONTACT RECEIVED AN UNKNOWN RECALL NOTICE FROM FORD MOTOR COMPANY A WEEK AFTER THE CRASH. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VIN WAS INVALID. THE FAILURE MILEAGE WAS 125,000.
TL* THE CONTACT OWNS A 2008 FORD F-350 SD. WHILE DRIVING APPROXIMATELY 12 MPH, THE STEERING FAILED WITHOUT WARNING. THE CONTACT STATED THAT THE STEERING WHEEL BECAME DETACHED FROM THE STEERING BOX. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE STEERING BOX NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. BOB BELL FORD WAS CONTACTED BY PHONE AT 410-766-3600 (LOCATED AT 7125 RITCHIE HWY, GLEN BURNIE, MD 21061). THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 125,000.
TL* THE CONTACT OWNS A 2008 FORD F-350 SD. WHILE DRIVING APPROXIMATELY 10 MPH, THE CONTACT HEARD AN ABNORMAL NOISE FROM THE FRONT OF THE VEHICLE. IN ADDITION, THE VEHICLE WENT INTO LIMP MODE. A LOCAL DEALER WAS NOT CONTACTED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND ADVISED THE CONTACT TO CALL NHTSA. THE APPROXIMATE FAILURE MILEAGE WAS 212,425. THE VIN WAS NOT AVAILABLE.
TL* THE CONTACT OWNS A 2008 FORD F-350. WHILE DRIVING 65 MPH AND ATTEMPTED TO EXIT THE HIGHWAY, THE STEERING WHEEL SEIZED AND THE BRAKE PEDAL WAS DEPRESSED, BUT THE BRAKES FAILED TO ENGAGE. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE DEALER WAS NOT CALLED FOR DIAGNOSTIC TESTING OR REPAIRS. THE CONTACT STATED THAT THE FAILURE RECURRED. THE CONTACT CALLED THE MANUFACTURER, BUT THERE WAS NO RESPONSE. THE FAILURE MILEAGE WAS APPROXIMATELY 104,000.
ENGINE DID NOT KICK OUT OF REGIN CAUSEING OVER HEAT
TRUCK WAS TAKEN TO FORD DEALER AND DIAGNOSED WITH LOW PRESSURE FUEL PUMP AND HIGH PRESSURE FUEL PUMP OUT.PRIOR TO THIS WHITE SMOKE ROLLED OUT OF EXHAUST WHILE DRIVING ON HIGHWAY AND ENGINE SHUT OFF.TRUCK WAA TOWED TO DEALER WITH ABOVE FINDINGS.FORD DIESEL MECHANIC STATED SEVERAL ISSUES WITH HIGH AND LOW PRESSURE FUEL PUMPS ON THESE MODELS.PLEASE LOOK INTO THIS.ESTIMATED COST IS 13,000 DOLLARS TO FIX.
TL* THE CONTACT OWNS A 2008 FORD F-350. THE CONTACT STATED THAT THE EXHAUST MANIFOLD DETACHED FROM THE HEAD OF THE ENGINE AND CAUSED EXHAUST FUMES TO ENTER THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO CONFIRMED THE FAILURE. THE DEALER WAS NOT CONTACTED. THE MANUFACTURER WAS CONTACTED AND ADVISED THE CONTACT TO TAKE THE VEHICLE TO A FORD DEALER. THE VIN WAS INVALID. THE FAILURE MILEAGE WAS APPROXIMATELY 53,000. ...UPDATED 10/19/17 *BF CONSUMER STATED MY INDEPENDENT MECHANIC CONFIRMED THE DRIVERS SINE EXHAUST MANIFORD HAD SEPARATED FROM THE HEAD BECAUSE ALL OF THE STUDS & KNOTS WERE RUSTED OFF. UPDATED 10/3/18*JB
STEERING GEARBOX FAILED. STEERING FELT VERY LOOSE, PULLED INTO PARKING LOT. STEERING WOULD TURN RIGHT BUT WOULD NOT TURN TO THE LEFT.COULD HEAR A CRUNCHING OR POPPING NOISE WHEN ATTEMPTING TOP TURN LEFT. HAD VEHICLE TOWED TO LOCAL REPAIR SHOP THAT FOUND THE STEERING GEARBOX FAILED INTERNALLY.
UPON RETURNING FROM A SHORT DRIVE I NOTICED OIL ON THE GROUND...HAD TRUCK TOWED TO LOCAL FORD DEALER ...WHEN INSPECTED I WAS INFORMED THE SELF CLEANING EXHAUST SYSTEM CAUSED THE RINGS TO WEAR PREMATURELY AND BUILD PRESSURE IN THE CRANKCASE CAUSING OIL TO SPEW OUT ANY OPENING IE THE DIPSTICK TUBE. A DIESEL ENGINE SHOULD HAVE BEEN EXPECTED TO LAST 2-3 TIMES THE 165,000 MILES ON THE TRUCK.
EXCESSIVE WHITE SMOKE OUT OF EXHAUST, ESPECIALLY WITH ACCELERATION. SMOKE HAS A FOUL ODOR ALSO. CAN HEAR A KNOCKING SOUND IN ENGINE ON DECELERATION (SIMILAR TO BAD WHEEL BEARING HUMS), ONLY DOES IT IF TURBO IS OVER 150-200 PSI, BUT WILL DO IT EVERY SINGLE TIME. 'DRIVE TO CLEAN EXHAUST' DISPLAYED ON DASH. COMPLETED RECOMMENDED DRIVE CYCLE (OVER 30MPH FOR AT LEAST 20 MINUTES, I DROVE FOR 45 MINS) AND MESSAGE STILL APPEARS. "WRENCH" SYMBOL DISPLAYED ON DASH. PER OWNER'S GUIDE THE RTT DISPLAYS WHEN ENGINE HAS DEFAULTED TO "LIMP-HOME" OPERATION OR WHEN TRANSMISSION PROBLEM HAS BEEN DETECTED.. THE LIGHT COMES ON EVERY TIME VEHICLE IS DRIVING NOW, AND STAYS ON ENTIRE TIME.
TL* THE CONTACT OWNS A 2008 FORD F-350. WHILE DRIVING OVER A BUMP IN THE ROAD, THE VEHICLE SHOOK, BOUNCED, AND MADE A SQUEAKING NOISE. THE CONTACT CALLED SCHULTZ FORD LINCOLN (LOCATED AT 80 NU-304, NANUET, NY 10954, (877) 724-8589) AND WAS INFORMED TO CONTACT THE MANUFACTURER TO SEE IF THE VEHICLE WAS COVERED UNDER WARRANTY OR RECALLS. IN ADDITION, WHEN THE CONTACT CHECK UNDER THE VEHICLE, HE NOTICED THAT THE RUBBER BUSHING DISINTEGRATED FROM THE CAB AND CHASSIS. THE VEHICLE WAS NOT TAKEN TO A DEALER AND WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURES. THE CONTACT WAS INFORMED THAT THE VEHICLE WAS OUT OF WARRANTY AND THERE WERE NO RECALLS ASSOCIATED WITH THE VIN. THE APPROXIMATE FAILURE MILEAGE WAS 48,000.
NITTO DURA GRAPPLER 245/75R/17 FRONT LEFT TIRE BLEW CAUSING VEHICLE TO CRASH INTO GUARD RAILING ON INTERSTATE. THE VEHICLE WAS DRIVING ON I-75 SB NEAR MM 181 APPROXIMATELY 72 MPH. I WAS NOT MADE AWARE OF THE RECALL. ON MARCH 6,2015 I HAD ANOTHER TIRE BLOW AND I FILED A NITTO CLAIM NUMBER 804190 (THROUGH THE TIRE DEALERSHIP). I RECEIVED FROM NITTO THE SAME TIRE IN EXCHANGE. EVEN THOUGHT THIS TYPE OF TIRE WAS RECALLED ON SAFERCAR.GOV ON NOVEMBER 4, 2015. WHY WAS IT REPLACED BY NITTO WITH ANOTHER DEFECTIVE TIRE??? NOW MY VEHICLE IS TOTALED!
TL* THE CONTACT OWNS A 2008 FORD F-350. WHILE DRIVING 25 MPH, THE CONTACT HEARD AN ABNORMAL SOUND AND THE STEERING WHEEL FRACTURED WITHOUT WARNING. THE CONTACT WAS ABLE TO COAST INTO A PARKING LOT, WHERE THE VEHICLE WAS PARKED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VIN WAS UNKNOWN. THE FAILURE MILEAGE WAS 215,000.
TL* THE CONTACT OWNS A 2008 FORD F-350. WHILE DRIVING APPROXIMATELY 55 MPH, THE STEERING WHEEL AND BRAKING ABILITY SEIZED AND BECAME DIFFICULT TO MANEUVER WITHOUT WARNING. THE FAILURE RECURRED SEVERAL TIMES. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 118,000.
TL* THE CONTACT OWNS A 2008 FORD F-350 SD. THE CONTACT STATED THAT THE VEHICLE EXPERIENCED A RANDOM DEATH WOBBLE ASSOCIATED WITH THE STEERING AND SUSPENSION. A DEALER PERFORMED EXTENSIVE REPAIRS, BUT THE CONDITION CONTINUED. THE DEALER AND THE MANUFACTURER FAILED TO PROVIDE A REMEDY. THE VEHICLE WAS UNABLE TO BE SAFELY DRIVEN DUE TO A STRONG VIBRATION FROM THE STEERING, WHICH ALSO CAUSED THE SUSPENSION TO BE UNSTABLE. THE VEHICLE WAS PARKED AT THE CONTACT'S RESIDENCE. THE FAILURE MILEAGE WAS NOT AVAILABLE.
I NOTICED A PLUM OF WHITE SMOKE OUT THE TAIL PIPE. THAT INDICATED STEAM, WATER IN THE SYSTEM TO ME. ALL THE GAUGES WERE NORMAL AND I STOPPED THE VEHICLE AND CHECKED THE FLUID LEVELS. NO OBVIOUS PROBLEM. I CALLED MY LOCAL FORD DEALERSHIP AND THEY COULD NOT GET IT IN FOR 36 HOURS. I DROVE IT .4 MILES HOME AND PARKED IT. AT THE APPOINTED TIME I DROVE TO NORTH COUNTRY FORD. IT TOOK THEM ANOTHER DAY TO FIND THE DIESEL MECHANIC WHO COULD WORK ON THE VEHICLE. 24 HOURS LATER I AM TOLD THE ENGINE IS BLOWN; FLUID GOT INTO THE MANIFOLD AND WAS SUCKED INTO THE # 3 CYLINDER. DEPENDING ON THE AMOUNT OF PARTS THAT COULD BE SALVAGED THE COST OF REPLACEMENT COULD EXCEED $ 12,000. THIS VEHICLE HAS 95,000 MILES ON IT. IT HAS HAD TOW OTHER INCIDENTS WITH THE ENGINE AND DRIVE TRAIN: IN DECEMBER OF LAST YEAR, IN PREPARATION FOR A TRIP TO ARIZONA I HAD THE TRANSMISSION SERVICED. ABOUT 1400 MILES LATER THE TRANSMISSION BEGAN TO SLIP WHEN WE ENCOUNTERED ANY HILLS OR MOUNTAINS. I PARKED THE TRAILER AND TOOK THE TUCK TO CASSA FORD. THEY HAD THE TRUCK FOR 4 DAYS AND $ 1600.00 WORTH OF REPAIRS. I ASKED IF ANYTHING DONE AT THE TIME IT WAS SERVICE OR THE DRIVING FROM THE FIRST SIGN OF TROUBLE HAD CAUSED OR EXACERBATED THE PROBLEM. THEY SAID NO, IT WAS A PUMP PROBLEM. IN 2011, IT BEGAN TO BLOW BLACK SMOKE OUT THE TAILPIPE; THE DASH SCREEN INDICATED IT WAS CLEANING THE EXHAUST. WITHIN 5 MINUTES THE ENGINE SPUTTERED AND DIED. I CALLED FORD I WAS TOLD TO WAIT AN HOUR AND TRY TO RESTART THE VEHICLE; GIVE THE ENGINE AN OPPORTUNITY TO 'RE-SET' ITSELF. THAT DIDN'T WORK! A TOW WAS SENT AND THE VEHICLE TOWED TO NELSON FORD DEALER IN FERGUS FALLS, MINNESOTA. IT WAS A FAILED EGR VALVE. THE REPAIR WAS COVERED UNDER WARRANTY.
TL* THE CONTACT OWNS A 2008 FORD F-350 SD EQUIPPED WITH BF GOODRICH RUGGED TERRAIN T/A TIRES, SIZE: 275/70R18. WHILE DRIVING APPROXIMATELY 50 MPH, THE TIRE TREAD DETACHED FROM THE FRONT DRIVER SIDE TIRE. VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS CONFIRMED THAT THE TREAD SEPARATED FROM THE TIRE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VEHICLE FAILURE MILEAGE WAS 91,335 AND THE TIRE FAILURE MILEAGE WAS APPROXIMATELY 3,000.
I RECENTLY PURCHASED A 2008 FORD F350 DIESEL CREW CAB PICKUP FROM HAYFORD FORD IN ISANTI MN. I HAVE DRIVEN THE VEHICLE A TOTAL OF 1500 MILES SINCE I PURCHASED IT. THE VEHICLE HAS BEEN IN THE SHOP MORE THAN 20 DAYS SINCE I PURCHASED IT. THEY NOW SAY I WILL HAVE A BILL OF $8000 DOLLARS TO REPAIR THE CONTAMINATED DIESEL FUEL SYSTEM. I UNDERSTAND THAT THERE HAS BEEN A FUEL TANK DELAMINATION ISSUE ON THESE VEHICLES THAT CAUSES THIS PROBLEM. THAT CAN LEAD TO A STALLING OF THE ENGINE IF NOT DETECTED PRIOR TO TOTAL FAILURE. FORD WILL NOT EVEN HONOR THE WARRANTY I PURCHASED FROM THEM. I NOTICED THE INCREASE IN ENGINE OIL VOLUME PRIOR TO ANY FAILURE WHICH LED FORD TO DIAGNOSE A FUEL PUMP FAILURE PRIOR TO ENGINE FAILURE. I UNDERSTAND THERE HAVE BEEN FAILURES WHILE THE VEHICLES ARE IN MOTION, WHICH WOULD CAUSE THE POSSIBILITY OF SERIOUS ACCIDENTS.
MY WIFE DROVE THE TRUCK TO WORK. SHE SAID IT WAS ACTING WEIRD. IT HAD SLACK GOING TO THE RIGHT. IT WAS HARD TO TURN TO THE LEFT. WHEN SHE GOT HOME IT WAS WORSE. I OPENED THE HOOD TO CHECK IT FOR FLUID.THE FLUID WAS GOOD. I GOT INSIDE TO CHECK OUT THE STEERING. IT HAD A LOT OF SLACK BOTH DIRECTIONS. AFTER A FEW TURNS THE HORN WENT OFF AND I HAD TO DISCONNECT THE BATTERY IN ORDER TO GET IT TO GO OFF. I THEN TRIED TO TURN THE STEERING AGAIN. I COULD HEAR SOME GRINDING FROM THE GEAR BOX. I DISCONNECTED THE HORN AND RECONNECTED THE BATTERY. I STARTED THE TRUCK AND ATTEMPTED TO TURN THE STEERING WHEEL AGAIN. THIS TIME FLUID STARTED TO SPRAY ALL OVER. I COULDN'T LOCATE THE SOURCE. I BELIEVE THAT THERE IS A PROBLEM IN THE GEAR BOX. I DON'T KNOW WHY THE HORN WENT OFF. IT IS NOT ABLE TO BE DRIVEN. IT IS IN MY DRIVEWAY PARKED. ALL I KNOW IS THAT IF IT HAD GONE OUT WHEN MY WIFE WAS ON THE HIGHWAY ONLY GOD KNOWS WHAT WOULD HAVE HAPPENED. SHE TAKES OUR THREE CHILDREN TO DAY CARE. THIS IS THE ONLY VEHICLE THAT IS BIG ENOUGH TO CARRY THE ENTIRE FAMILY. THE TRUCK HAS ONLY 91000 MILES. I LOOKED IT UP AND THERE HAS BEEN OTHER COMPLAINTS WITH THIS YEAR AND MODEL. WE DON'T KNOW HOW MUCH THIS IS GOING TO COST. MY VIEW IS THAT IT IS A DEFECT IN THE TRUCK THAT WAS KNOWN AND WE WERE NOT NOTIFIED OF ANY POSSLBLE PROBLEMS. IT IS SATURDAY NIGHT AND WE CANT CALL FORD GARAGE TILL MONDAY. WE WILL CALL AND ASK THEM WHAT WE CAN DO.
TL* THE CONTACT OWNS A 2008 FORD F-350 SD. WHILE DRIVING VARIOUS SPEEDS, THE BRAKE PEDAL WAS DEPRESSED AND THE POWER STEERING LOST POWER AND BECAME DIFFICULT TO OPERATE. THE VEHICLE WAS DIAGNOSED BY AN INDEPENDENT MECHANIC WHO STATED THAT A BOLT IN THE POWER STEERING MECHANISM FRACTURED AND NEEDED TO BE REPAIRED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 110,000. UPDATED 09/06/16*LJ UPDATED 09/08/16.*JB
BED RAILS ARE ROTTING PREMATURELY CAUSING SAFETY CONCERN WHEN TRUCK IS TOWING OR THERE IS WEIGHT IN THE BED OF THE TRUCK I FEEL THAT THIS MAY CAUSE A SAFETY ISSUE FOR PASSENGERS IN THE TRUCK AS WELL AS OTHER MOTORIST ON THE ROADWAY. FIFTH WHEEL HITCH CONNECTION SHIFT BECAUSE OF ROTTED RAIL CAUSING JAM IN HITCH CREATING TRAVEL HAZARD